Киосера ошибка 1010

Модератор: vetal


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Сообщение dviz » Вт дек 30, 2014 2:15 pm

Последний раз редактировалось dviz Вт дек 30, 2014 2:15 pm, всего редактировалось 1 раз.


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Сообщение S S S » Вт дек 30, 2014 2:17 pm

Изменить размер шрифта ↓ВернутьИзменить размер шрифта ↑

dviz писал(а):Смотри механизм подъёма бумаги в лотке — сам лоток может заклинило или шестерни или движок.

совершенно верно, шестерня вылетела из пазов, благодарю!
при дальнейшем осмотре выяснилось ещё что сам механизм который подходит к шестерне сломан.

S S S

  

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Вернуться в Принтеры, МФУ, факсы, копиры формата A4

Кто сейчас на форуме

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Все современные копировальные аппараты, мфу и принтеры Kyocera имеют возможность диагностировать все узлы устройства в режиме запуска и во время работы аппарата. По этому, если во время включения или во время работы произошел сбой, то техника Kyocera сможет сообщить о наличии ошибки.

В большинстве случаев у аппаратов Kyocera код ошибки отображается на дисплее, в остальных случаях тип ошибки зависит от последовательности и количества миганий индикаторов.
Если Ваш копировальный аппарат, МФУ или принтер Kyocera выдал на дисплее некий код, то узнать причину, описание возникновения ошибки, а так же в каком узле аппарата стоит искать проблему, Вы можете в этом разделе выбрав интересующую модель из списка.

Но диагностика не решит проблему сбоя аппарата, для этого лучше обратиться к профессиональным и опытным сервисным специалистам компании Kyomart! Позвоните нам по телефону
8 (343) 288-23-45 или отправьте запрос на электронную почту: sales@kyomart.ru , и мы обязательно свяжемся с Вами в кратчайшие сроки.

Код ошибки Описание ошибки Причина ошибки
0100 Backup memory device error Defective flash memory. Defective main PWB.
0120 MAC address data error
For data in which the MAC address is invalid.
Defective flash memory. Defective engine PWB.
0130 Backup memory read/write error Defective flash memory. Defective control PWB.
0140 Backup memory data error Defective flash memory. Defective control PWB.
0150 Control PWB EEPROM error
Detecting control PWB EEPROM (U17) communication error.
Improper installation control PWB EEPROM (U17). Defective control PWB. Data damage of control PWB EEPROM (U17).
0170 Billing counting error Defective control PWB. Data damage of control PWB EEPROM (U17).
0190 Backup memory device error (engine PWB) Defective engine PWB.
0800 Image processing error
JAM010x is detected twice.
Defective main PWB.B.
0840 Faults of RTC
The time is judged to go back based on the comparison of the RTC time and the current time or five years or more have passed.
Defective control PWB. The battery is disconnected from the control PWB.
1010 Lift motor error
During driving the lift motor, a motor overcurrent signal is detected for 5 s. This error is detected five times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the lift motor. Defective lift motor. Defective engine PWB or connect-R PWB.
1020 PF lift motor 1 error (paper feeder)
After cassette 2 is inserted, PF lift sensor 1 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1030 PF lift motor 2 error (paper feeder)
After cassette 3 is inserted, PF lift sensor 2 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1040 PF lift motor 3 error (paper feeder)
After cassette 4 is inserted, PF lift sensor 3 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1050 PF lift motor 4 error (paper feeder)
After cassette 5 is inserted, PF lift sensor 4 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1140 BPF lift motor upward error (Bulk paper feeder)
BPF lift maximum sensor does not turn on. The lock signal of the motor is detected continuously three times.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the motor. Defective BPF lift motor. Defective BPF main PWB.
1150 BPF lift motor downward error (Bulk paper feeder)
BPF lift minimum sensor does not turn on. The lock signal of the motor is detected continuously three times.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the motor. Defective BPF lift motor. Defective BPF main PWB.
1800 Paper feeder 1 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective engine PWB. Defective PF main PWB.
1810 Paper feeder 2 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective PF main PWB.
1820 Paper feeder 3 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective PF main PWB.
1830 Paper feeder 4 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective PF main PWB.
1900 Paper feeder 1/BPF paper feeder EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
1910 Paper feeder 2 EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
1920 Paper feeder 3 EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
1930 Paper feeder 4 EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
2000 Main motor error
The main motor ready input is not given for 2 s during the main motor is ON.
Defective harness between main motor (CN1) and control PWB (YC17), or improper connector insertion. Defective drive transmission system of the main motor. Defective main motor. Defective control PWB.
2010 Main motor steady-state error
Stable OFF is detected for 2 s continuously after main motor stabilized.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the main motor. Defective main motor. Defective engine PWB.
2200 Drum motor steady-state error
The drum motor ready input is not given for 2 s during the drum motor is ON.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the drum motor. Defective drum motor. Defective engine PWB.
2210 Drum motor steady-state error (60/50/45 ppm model only)
Stable OFF is detected for 2 s continuously after drum motor stabilized.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the drum motor. Defective drum motor. Defective engine PWB.
2330 Fuser pressure release motor error (Over-current) (60/50/45 ppm model only)
The over-current detection signal of the motor is detected continuously twenty times.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the fuser pressure release motor. Defective fuser pressure release motor. Defective PWB.
2340 Fuser pressure release motor error (Timeout) (60/50/45 ppm model only)
The position detection sensor is not detected continuously for 30 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the fuser pressure release motor. Defective fuser pressure release motor. Defective PWB.
2600 PF drive motor 1 error (paper feeder 1)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
2610 PF drive motor 2 error (paper feeder 2)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
2620 PF drive motor 3 error (paper feeder 3)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
2630 PF drive motor 4 error (paper feeder 4)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
4000 Polygon motor (laser scanner unit) error
The polygon motor ready input is not given for 6 s during the polygon motor is ON.
Defective harness between polygon motor and control PWB (YC10), or improper connector insertion. Defective laser scanner unit. Defective control PWB.
4200 BD error (laser scanner unit) error BD sensor does not detect laser beam due to condensation on the polygon mirror. Defective laser scanner unit. Defective control PWB.
5100 Main charger high-voltage error
Five pages have been printed with the main charger output short-circuited.
Drum unit installed incorrectly. Engine PWB installed incorrectly. Defective engine PWB.
6000 Broken fuser heater wire
The temperature does not reach 100°C/212°F after the fuser heater has been turned on continuously for 30 s. The temperature does not rise by 1°C/1.8°F after the fuser heater lamp has been turned on continuously for 15 s during warm-up or at standby.(Only when the detection temperature is less than 200°C.)
Defective connector cable or poor contact in the connector. Fuser thermostat triggered. Broken fuser heater wire.
6020 Abnormally high fuser thermistor temperature
Fuser thermistor detects abnormally temperature.
Shorted fuser thermistor. Defective control PWB.
6030 Broken fuser thermistor wire
Input from fuser thermistor is 0 (A/D value).
Poor contact in the fuser thermistor connector terminals. Broken fuser thermistor wire. Fuser thermistor installed incorrectly. Fuser thermal cutout triggered. Fuser heater lamp installed incorrectly. Broken fuser heater lamp wire.
6120 Abnormally high fuser thermistor 1 temperature
(60/50/45 ppm model) The detection temperature of fuser thermistor 1 is higher than 245°C/473°F. In a heater-off state, the detection temperature of fuser thermistor 1 is higher than 195°C/383°F after the detection temperature of fuser thermistor 1 was 155°C/311°F or less. (40 ppm model) The detection temperature of fuser thermistor 1 is higher than 250°C/482°F. In a heater-off state, the detection temperature of fuser thermistor 1 is higher than 170°C/338°F after the detection temperature of fuser thermistor 1 was 155°C/311°F or less.
Deformed connector pin. Defective triac. Shorted fuser thermistor. Defective engine PWB.
6130 Broken fuser thermistor 1 wire
A/D value of the fuser thermistor 1 exceeds 1019 bit continuously for 4 s during warming up.
Defective connector cable or poor contact in the connector. Deformed connector pin. Defective triac.or pin. Defective fuser thermistor. Defective engine PWB.
6400 Zero cross signal error
The zero cross signal does not reach the control PWB for specified time.
Defective harness between high voltage PWB (YC202) and control PWB (YC23), or improper connector insertion. Defective connection between power source PWB (YC103) and high voltage PWB (YC201). Defective power source PWB. Defective control PWB.
7000 Toner motor lock error
During driving the toner motor, a motor overcurrent signal is detected for 5 s.
Lump of toner inside toner container. Defective drive transmission system of the toner motor. Defective toner motor. Defective engine PWB.
7100 Toner sensor error
Sensor output value of 930 or more continuously for 5 s.
Defective connector cable or poor contact in the connector. Defective toner sensor. Defective engine PWB.
7400 Developer unit non-installing error
Sensor output value of 31 or less continuously for 5 s.r.
Defective connector cable or poor contact in the connector. Defective toner sensor. Defective engine PWB.
7410 Drum unit non- installing error The drum unit is not installed or not installed properly. The drum PWB EEPROM does not communicate normally. The drum unit is not installed. Defective connector cable or poor contact in the connector. Defective drum PWB EEPROM. Defective engine PWB.
7800 Broken external thermistor wire
The average of thermistor output value of 1016 or more continuously for 160 ms. The average of thermistor output value of 930 or more continuously for 5 s.
Defective connector cable or poor contact in the connector. Defective temperature sensor.
7810 Short-circuited external thermistor wire
The average of thermistor output value of 31 or less continuously for 5 s.
Defective connector cable or poor contact in the connector. Defective temperature sensor.
7900 Drum unit EEPROM error
No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs eight times successively. Mismatch between writing data and reading data occurs eight times successively.
Defective connector cable or poor contact in the connector. Defective drum unit.
F000 Main PWB — operation panel PWB communication error Defective main PWB. Defective operation panel PWB.
F010 Main PWB checksum error Defective main PWB.
F020 Main PWB RAM checksum error Defective main memory (RAM) on the main PWB. Defective expanded memory (DIMM).
F040 Main PWB — engine PWB communication error Defective main PWB. Defective engine PWB.
F041 Main PWB — scanner communication error Defective main PWB.
F050 Engine ROM checksum error Defective engine PWB.
F051 Scan engine ROM checksum error Defective engine PWB.

Модератор: vetal


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Сообщение dviz » Вт дек 30, 2014 2:15 pm

Последний раз редактировалось dviz Вт дек 30, 2014 2:15 pm, всего редактировалось 1 раз.


За это сообщение автора dviz поблагодарил:
S S S
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dviz

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Сообщение S S S » Вт дек 30, 2014 2:17 pm

Изменить размер шрифта ↓ВернутьИзменить размер шрифта ↑

dviz писал(а):Смотри механизм подъёма бумаги в лотке — сам лоток может заклинило или шестерни или движок.

совершенно верно, шестерня вылетела из пазов, благодарю!
при дальнейшем осмотре выяснилось ещё что сам механизм который подходит к шестерне сломан.

S S S

Испачкался тонером

  • Не в сети
  • ICQ
  • Персональный альбом


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Вернуться в Принтеры, МФУ, факсы, копиры формата A4

Кто сейчас на форуме

Сейчас этот форум просматривают: нет зарегистрированных пользователей и гости: 45


Все современные копировальные аппараты, мфу и принтеры Kyocera имеют возможность диагностировать все узлы устройства в режиме запуска и во время работы аппарата. По этому, если во время включения или во время работы произошел сбой, то техника Kyocera сможет сообщить о наличии ошибки.

В большинстве случаев у аппаратов Kyocera код ошибки отображается на дисплее, в остальных случаях тип ошибки зависит от последовательности и количества миганий индикаторов.
Если Ваш копировальный аппарат, МФУ или принтер Kyocera выдал на дисплее некий код, то узнать причину, описание возникновения ошибки, а так же в каком узле аппарата стоит искать проблему, Вы можете в этом разделе выбрав интересующую модель из списка.

Но диагностика не решит проблему сбоя аппарата, для этого лучше обратиться к профессиональным и опытным сервисным специалистам компании Kyomart! Позвоните нам по телефону
8 (343) 288-23-45 или отправьте запрос на электронную почту: sales@kyomart.ru , и мы обязательно свяжемся с Вами в кратчайшие сроки.

Код ошибки Описание ошибки Причина ошибки
0100 Backup memory device error Defective flash memory. Defective main PWB.
0120 MAC address data error
For data in which the MAC address is invalid.
Defective flash memory. Defective engine PWB.
0130 Backup memory read/write error Defective flash memory. Defective control PWB.
0140 Backup memory data error Defective flash memory. Defective control PWB.
0150 Control PWB EEPROM error
Detecting control PWB EEPROM (U17) communication error.
Improper installation control PWB EEPROM (U17). Defective control PWB. Data damage of control PWB EEPROM (U17).
0170 Billing counting error Defective control PWB. Data damage of control PWB EEPROM (U17).
0190 Backup memory device error (engine PWB) Defective engine PWB.
0800 Image processing error
JAM010x is detected twice.
Defective main PWB.B.
0840 Faults of RTC
The time is judged to go back based on the comparison of the RTC time and the current time or five years or more have passed.
Defective control PWB. The battery is disconnected from the control PWB.
1010 Lift motor error
During driving the lift motor, a motor overcurrent signal is detected for 5 s. This error is detected five times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the lift motor. Defective lift motor. Defective engine PWB or connect-R PWB.
1020 PF lift motor 1 error (paper feeder)
After cassette 2 is inserted, PF lift sensor 1 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1030 PF lift motor 2 error (paper feeder)
After cassette 3 is inserted, PF lift sensor 2 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1040 PF lift motor 3 error (paper feeder)
After cassette 4 is inserted, PF lift sensor 3 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1050 PF lift motor 4 error (paper feeder)
After cassette 5 is inserted, PF lift sensor 4 does not turn on. This error is detected four times successively.
Defective bottom plate elevation mechanism in the cassette. Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF lift motor. Defective PF lift motor. Defective PF main PWB.
1140 BPF lift motor upward error (Bulk paper feeder)
BPF lift maximum sensor does not turn on. The lock signal of the motor is detected continuously three times.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the motor. Defective BPF lift motor. Defective BPF main PWB.
1150 BPF lift motor downward error (Bulk paper feeder)
BPF lift minimum sensor does not turn on. The lock signal of the motor is detected continuously three times.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the motor. Defective BPF lift motor. Defective BPF main PWB.
1800 Paper feeder 1 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective engine PWB. Defective PF main PWB.
1810 Paper feeder 2 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective PF main PWB.
1820 Paper feeder 3 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective PF main PWB.
1830 Paper feeder 4 communication error
A communication error is detected 10 times in succession.
Improper installation paper feeder. Defective connector cable or poor contact in the connector. Defective PF main PWB.
1900 Paper feeder 1/BPF paper feeder EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
1910 Paper feeder 2 EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
1920 Paper feeder 3 EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
1930 Paper feeder 4 EEPROM error
When writing the data, the write data and the read data is not in agreement.
Defective PF main PWB. Device damage of EEPROM.
2000 Main motor error
The main motor ready input is not given for 2 s during the main motor is ON.
Defective harness between main motor (CN1) and control PWB (YC17), or improper connector insertion. Defective drive transmission system of the main motor. Defective main motor. Defective control PWB.
2010 Main motor steady-state error
Stable OFF is detected for 2 s continuously after main motor stabilized.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the main motor. Defective main motor. Defective engine PWB.
2200 Drum motor steady-state error
The drum motor ready input is not given for 2 s during the drum motor is ON.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the drum motor. Defective drum motor. Defective engine PWB.
2210 Drum motor steady-state error (60/50/45 ppm model only)
Stable OFF is detected for 2 s continuously after drum motor stabilized.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the drum motor. Defective drum motor. Defective engine PWB.
2330 Fuser pressure release motor error (Over-current) (60/50/45 ppm model only)
The over-current detection signal of the motor is detected continuously twenty times.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the fuser pressure release motor. Defective fuser pressure release motor. Defective PWB.
2340 Fuser pressure release motor error (Timeout) (60/50/45 ppm model only)
The position detection sensor is not detected continuously for 30 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the fuser pressure release motor. Defective fuser pressure release motor. Defective PWB.
2600 PF drive motor 1 error (paper feeder 1)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
2610 PF drive motor 2 error (paper feeder 2)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
2620 PF drive motor 3 error (paper feeder 3)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
2630 PF drive motor 4 error (paper feeder 4)
When the PF drive motor is driven, error signal is detected continuously for 2 s.
Defective connector cable or poor contact in the connector. Defective drive transmission system of the PF drive motor. Defective PF drive motor. Defective PF main PWB.
4000 Polygon motor (laser scanner unit) error
The polygon motor ready input is not given for 6 s during the polygon motor is ON.
Defective harness between polygon motor and control PWB (YC10), or improper connector insertion. Defective laser scanner unit. Defective control PWB.
4200 BD error (laser scanner unit) error BD sensor does not detect laser beam due to condensation on the polygon mirror. Defective laser scanner unit. Defective control PWB.
5100 Main charger high-voltage error
Five pages have been printed with the main charger output short-circuited.
Drum unit installed incorrectly. Engine PWB installed incorrectly. Defective engine PWB.
6000 Broken fuser heater wire
The temperature does not reach 100°C/212°F after the fuser heater has been turned on continuously for 30 s. The temperature does not rise by 1°C/1.8°F after the fuser heater lamp has been turned on continuously for 15 s during warm-up or at standby.(Only when the detection temperature is less than 200°C.)
Defective connector cable or poor contact in the connector. Fuser thermostat triggered. Broken fuser heater wire.
6020 Abnormally high fuser thermistor temperature
Fuser thermistor detects abnormally temperature.
Shorted fuser thermistor. Defective control PWB.
6030 Broken fuser thermistor wire
Input from fuser thermistor is 0 (A/D value).
Poor contact in the fuser thermistor connector terminals. Broken fuser thermistor wire. Fuser thermistor installed incorrectly. Fuser thermal cutout triggered. Fuser heater lamp installed incorrectly. Broken fuser heater lamp wire.
6120 Abnormally high fuser thermistor 1 temperature
(60/50/45 ppm model) The detection temperature of fuser thermistor 1 is higher than 245°C/473°F. In a heater-off state, the detection temperature of fuser thermistor 1 is higher than 195°C/383°F after the detection temperature of fuser thermistor 1 was 155°C/311°F or less. (40 ppm model) The detection temperature of fuser thermistor 1 is higher than 250°C/482°F. In a heater-off state, the detection temperature of fuser thermistor 1 is higher than 170°C/338°F after the detection temperature of fuser thermistor 1 was 155°C/311°F or less.
Deformed connector pin. Defective triac. Shorted fuser thermistor. Defective engine PWB.
6130 Broken fuser thermistor 1 wire
A/D value of the fuser thermistor 1 exceeds 1019 bit continuously for 4 s during warming up.
Defective connector cable or poor contact in the connector. Deformed connector pin. Defective triac.or pin. Defective fuser thermistor. Defective engine PWB.
6400 Zero cross signal error
The zero cross signal does not reach the control PWB for specified time.
Defective harness between high voltage PWB (YC202) and control PWB (YC23), or improper connector insertion. Defective connection between power source PWB (YC103) and high voltage PWB (YC201). Defective power source PWB. Defective control PWB.
7000 Toner motor lock error
During driving the toner motor, a motor overcurrent signal is detected for 5 s.
Lump of toner inside toner container. Defective drive transmission system of the toner motor. Defective toner motor. Defective engine PWB.
7100 Toner sensor error
Sensor output value of 930 or more continuously for 5 s.
Defective connector cable or poor contact in the connector. Defective toner sensor. Defective engine PWB.
7400 Developer unit non-installing error
Sensor output value of 31 or less continuously for 5 s.r.
Defective connector cable or poor contact in the connector. Defective toner sensor. Defective engine PWB.
7410 Drum unit non- installing error The drum unit is not installed or not installed properly. The drum PWB EEPROM does not communicate normally. The drum unit is not installed. Defective connector cable or poor contact in the connector. Defective drum PWB EEPROM. Defective engine PWB.
7800 Broken external thermistor wire
The average of thermistor output value of 1016 or more continuously for 160 ms. The average of thermistor output value of 930 or more continuously for 5 s.
Defective connector cable or poor contact in the connector. Defective temperature sensor.
7810 Short-circuited external thermistor wire
The average of thermistor output value of 31 or less continuously for 5 s.
Defective connector cable or poor contact in the connector. Defective temperature sensor.
7900 Drum unit EEPROM error
No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs eight times successively. Mismatch between writing data and reading data occurs eight times successively.
Defective connector cable or poor contact in the connector. Defective drum unit.
F000 Main PWB — operation panel PWB communication error Defective main PWB. Defective operation panel PWB.
F010 Main PWB checksum error Defective main PWB.
F020 Main PWB RAM checksum error Defective main memory (RAM) on the main PWB. Defective expanded memory (DIMM).
F040 Main PWB — engine PWB communication error Defective main PWB. Defective engine PWB.
F041 Main PWB — scanner communication error Defective main PWB.
F050 Engine ROM checksum error Defective engine PWB.
F051 Scan engine ROM checksum error Defective engine PWB.

Индикатор ошибки на Kyocera TASKalfa 1800/2200Если с аппаратом Kyocera TASKalfa 1800, Kyocera TASKalfa 2200 произошла проблема, откроется следующий экран с уведомлением.
• Индикатор [Внимание] на панели управления горит или мигает.
• На дисплее сообщений панели управления аппарата появилось сообщение об ошибке.

Если индикатор [Внимание] горит или мигает и на дисплее сообщений панели управления аппарата появилось сообщение об ошибке, проверьте KYOCERA Client Tool или Монитор состояния.

ПРИМЕЧАНИЕ Если индикаторы постоянно горят и мигают не так, как описано выше, вероятно, произошла ошибка службы. Выключите питание, отсоедините шнур питания и вставьте его обратно, после чего включите питание. Это может помочь сбросить ошибку. Если ошибка не исчезает, свяжитесь со своим представителем сервисной службы (тел. в Минске +375 17 291-28-24)

Ниже описаны неполадки, которые не могут быть устранены пользователем

Дисплей сообщений

Описание

Меры устранения

Бункер отраб тонера перепол. или не уст.

Бункер для отработанного тонера установлен неправильно

Установите Бункер для отработанного тонера должным образом

Бункер для отработанного тонера заполнен

Замените бункер отработанного тонера

Встряхните картр. с тонером

Тонер слежался

Откройте переднюю крышку аппарата и вытяните контейнер с тонером. Сильно встряхните контейнер с тонером и установите его на место

Вызовите сервисный персонал.

В аппарате произошла ошибка

Обратите внимание на код ошибки, отображаемый в дисплее сообщений, и свяжитесь с представителем сервисной службы (тел. в Минске +375 17 291-28-24)

Выньте бумагу с внутреннего лотка

 

Извлеките бумагу из внутреннего лотка. Нажмите клавишу [OK], чтобы возобновить печать

Добавьте тонер

Закончился тонер

Замените контейнер с тонером TK-4105

Загрузите бумагу в кассету #

↑↓ (отображается попеременно)
A4 (формат бумаги)
Обычная (тип носителя)
OK: Перейдите к следующему шагу

Загрузите бумагу. Нажмите клавишу [OK] и перейдите к следующему шагу. • Для выбора другого устройства подачи выберите [Выберите бумагу]. • Для печати на бумаге, в настоящее время находящейся в устройстве подачи, выберите [Продолж. без изм.]

Загрузите бумагу в универсальный лоток

↑↓ (отображается попеременно)
A4 (формат бумаги)
Обычная (тип носителя)
OK: Перейдите к следующему шагу

Загрузите бумагу. Нажмите клавишу [OK] и перейдите к следующему шагу. • Для выбора другого устройства подачи выберите [Выберите бумагу]. • Для печати на бумаге, в настоящее время находящейся в устройстве подачи, выберите [Продолж. без изм.]

Закройте автоподатчик оригиналов

Открыт автоподатчик оригиналов

Откройте и закройте автоподатчик оригиналов

Закройте крышку автопод. оригиналов

Открыта верхняя крышка автоподатчика оригиналов

Откройте и закройте крышку автоподатчика оригинало

Закройте переднюю крышку

Открыта передняя крышка

Откройте и закройте переднюю крышку

Закройте правую крышку #

Открыта какая-либо крышка

Откройте и закройте крышку, обозначенную на экране

Замятие бумаги. (DP)
↑↓ (отображается попеременно)
Проверьте (B)(C) в крышке DP

В автоподатчике произошло замятие бумаги.

См. Устранение замятия бумаги в Руководстве по эксплуатации и извлеките замятую бумагу

Замените МК

Необходимо производить замену деталей комплекта техобслуживания MK-4105 (ремкомплекта) каждые 150 000 страниц печати.

Данная операция должна производиться специалистом. Обратитесь к представителю сервисной службы (тел. в Минске +375 17 291-28-24)

Замятие

Произошло замятие бумаги в кассете или универсальном лотке

См. Устранение замятия бумаги и извлеките замятую бумагу

Извлеките оригиналы из автоподатчика

Для продолжения работы необходимо извлечь оригиналы из автоподатчика оригиналов

Извлеките оригиналы из автоподатчика оригиналов

Кабель USB был отключен

Кабель USB не подключен

Нажмите клавишу [OK] и подключите кабель USB

ПК выключен

Нажмите клавишу [OK] и включите ПК

Не удается найти KYOCERA Client Tool

Нажмите клавишу [OK] и откройте KYOCERA Client Tool на ПК

Макс. к-во сканируемых страниц

Превышен предел сканирования

Дальнейшее сканирование невозможно. Задание отменено. Нажмите клавишу [OK]

Мало тонера. (Зам., когда законч.)

Скоро понадобится заменить контейнер с тонером 

Получите новый контейнер с тонером TK-4105. 
Внимание! Когда заканчивается тонер аппарат перестает печатать

Не оригинальный тонер

Установлен контейнер с тонером не марки Kyocera

Производитель не несет ответственности за повреждения, вызванные использованием неоригинального тонера. Мы рекомендуем использовать исключительно оригинальные контейнеры с тонером  TK-4105. .
Если нужно использовать установленный в настоящее время контейнер с тонером, нажмите одновременно и удерживайте клавиши [OK] и [Стоп] в течение не менее 3 с.

Неверный ид. уч. зап. Задание отменено

Указан неверный идентификатор учетной записи при внешней обработке задания. Задание отменено

Нажмите клавишу [OK]

Невозможна двусторонняя печать на этой бумаге

Не возможна печать на бумаге выбранного формата или типа

Нажмите клавишу [OK] и перейдите к следующему шагу:
• Для выбора другого устройства подачи выберите пункт [Выберите бумагу].
• Чтобы печатать, не используя функцию двусторонней печати, выберите пункт [Продолж. без изм.].

Недостаточно памяти. Невозможно начать выполнение задания

Невозможно начать выполнение задания

Повторите попытку позже

Ограничено алгоритмом учета заданий(Печать)

Задание отменено, поскольку его выполнение ограничено функцией учета заданий

Нажмите клавишу [OK]

Ограничено алгоритмом учета заданий(Сканер)

Задание отменено, поскольку его выполнение ограничено функцией учета заданий

Нажмите клавишу [OK]

Очистите сканер

Произошло загрязнение сканера

Очистите щелевое стекло с помощью чистящей салфетки, поставляемой вместе с автоподатчиком оригиналов.

Ошибка. Выключить

Отключите и снова включите аппарат с помощью выключателя питания

Память переполнена

Невозможно продолжить выполнение задания из-за отсутствия свободной памяти

Измените разрешение печати с Быстр1200 до 600 dpi. См. Printer Driver User Guide

Память сканера переполнена

Дальнейшее сканирование невозможно из-за нехватки памяти сканера.

Для отмены задания нажмите [OK]

Перезагрузка печати. Задание отменено

Предупреждение. Недостаточно памяти принтера. Задание отменено

Нажмите клавишу [OK]

Превышено ограничение учета заданий

Превышено число распечаток из-за ограничения алгоритмом учета заданий. Достигнут предел печати

Это задание отменено. Нажмите клавишу [OK]

Уст.другую кассету

Выбрано «Сдвиг»

Для использования сдвига необходимо загрузить в другой лоток бумагу такого же формата, что и в выбранном устройстве подачи, но в другой ориентации

Установите все оригиналы обратно и нажмите клавишу [Старт].

Возникает при печати двусторонних документов в режиме ручной двусторонней печати

Извлеките оригиналы из автоподатчика оригиналов, расположите их в первоначальном порядке и положите обратно. Нажмите клавишу [OK], чтобы возобновить печать. Для отмены задания нажмите [Стоп]

Установлен неизвестный тонер. ПК

Региональная спецификация контейнера с тонером не соответствует спецификации аппарата

Установите оригинальный контейнер с тонером Замените контейнер с тонером TK-4105

Если при работе с копировальном аппаратом у вас возникли проблемы, и система выдает код ошибки, вы можете идентифицировать ее с помощью данной таблицы.
Коды ошибок Kyocera-Mita указаны для более поздних моделей копиров. Если вы являетесь владельцем более ранней модели, необходимо к трехзначному коду ошибки прибавить знак «0».

Общие ошибки
 

Код ошибки Описание
0030 Fax control PWB system problem
0070 Fax control PWB incompatibility detection problem
0100 Backup memory read/write problem (main board)
0110 Backup memory data problem (main board)
0120 Drum EEPROM read/write problem (для 2550)
0130 Backup memory read/write problem (main PCB EEPROM) (для 1650/2050/2550)
0140 Backup memory data problem (main PCB EEPROM) (для 1650/2050/2550)
0150 Backup memory read/write problem (engine board)
0160 Backup memory data problem (engine board)
0170 Accounting count problem
0180 Machine number mismatch
0210 Communication problem between the main board and engine board (для KM-1500/1620/2020/1635/2035/1650/2050/2550/6030/8030, FS-1018/1118)
Communication problem between the main board and operation board (для KM-1525/1530/2030/2530/3530/6230/4530/5530/6330/7530)
0240 Printer board PWB communication problem
0250 Scanner network board communication problem
0280 Communication problem between the fax control PWB and main PWB
0320 Side deck communication problem
0340 Finisher communication problem
0410 Optional DP communication problem
0420 Optional first paper feeder communication problem
Large paper deck /paper feed desk communication problem /Side deck communication problem
0440 Finisher communication problem
0450 Mailbox communication problem
0470 Switchback unit communication problem
0500 Optional second paper feeder communication problem
0510 Optional third paper feeder communication problem
0600 DIMM problem (для 2530/3530)
0610 Bitmap (DIMM) problem
0620 Memory input interface problem
0630 DMA problem
0640 Hard disk drive problem
0800 Image processing problem (JAM05 is detected twice)
0820 Fax control PCB CG ROM checksum error
0830 Flash ROM program area checksum error
0860 Fax control PCB software switch checksum error
0870 Fax control PWB to main PWB high capacity data transfer problem
0880 Fax control PWB program archive problem
0890 Fax control PCB CG font archive problem
0900 Fax software incompatibility detection problem
0920 Fax file system error
0960 Developer EEPROM read/write problem (для 2550/6030/8030)
1000 Exposure lamp problem
1010 Lift motor 1 error
1020 Lift motor 2 error
1030 Lift motor 3 error
1040 Lift motor 4 error
1100 Paper deck motor 1 problem [Drawer 3]
1110 Paper deck motor 2 problem [Drawer 4]
1120 Deck right lift position problem
1130 Deck left lift position problem
1140 Side deck lift motor (going up) problem
1150 Side deck lift motor (going down) problem
1160 Large paper deck (paper feed desk) sequence problem
1170 Large paper deck (paper feed desk) incorrect type problem
2000 Main motor problem
Image forming motor problem (для 6230/4530/5530/6330/7530)
2500 Paper feed motor problem
2550 Paper conveying motor problem (для 4530/5530)
2600 Deck conveying motor /desk drive motor problem
2640 Side deck drive motor problem
3100 Scanner carriage problem
3200 Exposure lamp problem
3300 Optical system (AGC) problem
4000 Polygon motor synchronization problem
4010 Polygon motor steady-state problem
4100 BD initialization (A) problem
4110 BD initialization (B) problem
4200 BD steady-state problem
5100 Main charger problem
5110 Transfer/separation high voltage problem
5300 Broken cleaning lamp wire
5500 Drum surface potential sensor problem 1
5510 Drum surface potential sensor problem 2
5600 Drum surface potential problem 1
5610 Drum surface potential problem 2
6000 Broken fixing heater wire
6020 Abnormally high fixing unit thermistor temperature
6030 Broken fixing unit thermistor
6050 Abnormally low fixing unit thermistor temperature
6100 Broken fixing heater wire
6200 Abnormally low fixing unit thermistor temperature
6300 Abnormally high fixing unit thermistor temperature
6400 Zero-crossing signal problem
6410 Fixing unit connector insertion problem
6420 Fixing fuse cut problem
6420 Broken fixing unit thermistor wire
7100 Toner sensor problem
7300 Broken external temperature thermistor wire (для KM-1505/1510/1810/4230/5230/6230)
Toner sensor problem/ Toner hopper problem (для KM-2530/3530/3035/4035/5035/6230/4530/5530/6330/7530/6030/8030)
7310 Short-circuited external temperature thermistor
7400 Image formation unit connector insertion problem
Developing unit connector insertion problem (для 2550)
7410 Drum unit connector insertion problem
7750 Drum type mismatch problem A (для 1635/2035)
7760 Drum type mismatch problem B (для 1635/2035)
7800 Broken external temperature thermistor
7810 Short-circuited external temperature thermistor

KM-1500, FS-1018/1118 (KM-1820)

Код ошибки Описание
0220 Communication problem between the main board and operation board (для 1018/1118)
F— Controller system error (для 1018/1118)
F010 ROM checksum error (для 1118)
F012
7980 Waste toner reservoir overflow problem (when the total number of copies is less than 100 thousand sheets)
7990 Waste toner reservoir overflow problem (when the total number of copies is 100 thousand sheets or more)

KM-1505/1510/1810/1525/1530/2030

Код ошибки Описание
0210 Printer board communication problem (для 1505/1510/1810)
0400 DIMM problem
0410 Bitmap problem
0430 DMA problem
1040 Optical system problem (AGC)

Kyocera-Mita 3035/4035/5035

Код ошибки Описание
0100 Operation unit PCB backup memory read/write error
0110 Operation unit PCB backup memory data problem
0210 MMI communication problem
0320 Energy save communication problem
7450 Image formation unit fuse cut problem

Kyocera Mita 4230/5230

Код ошибки Описание
0010 Memory copy PCB 1 communication problem
0030 Memory copy PCB 2 communication problem
0100 RAM/ROM problem
0220 Communication problem between the engine PCB and main PCB
0230 Scanner communication problem
0260 Memory copy PCB 1 communication problem
0320 Large paper deck communication problem /Paper feed desk communication problem
0360 Memory copy PCB 2 communication problem
0370 Communication microcomputer problem
1040 Optical system problem (AGC)
2100 Paper conveying motor problem
2200 Side registration motor problem
2300 Paper feed motor problem
2310 Desk drive motor problem
2410 Upper lift motor problem
2420 Lower lift motor problem
2430 Upper desk lift motor problem
2440 Lower desk lift motor problem
3320 Scanner watchdog problem
3400 Original detection position problem
7400 Toner hopper problem
9200 Deck paper conveying motor problem
9210 Paper deck motor 1 problem
9220 Paper deck motor 2 problem
9230 Right lift position problem
9240 Left lift position problem

Kyocera-Mita 6030/8030

Код ошибки Описание
0060 Main PWB type mismatch error
0130 Backup memory (EEPROM) device problem
0140 Backup memory (EEPROM) data problem
0220 Scanner communication problem
0330 Relay board communication problem
0460 Duplex unit communication problem
0470 Sheet inserter communication problem (optional document finisher)
0500 Paper feed unit communication error (cassette 1 and 2)
0510 Paper feed unit communication error (cassette 3 and 4)
0700 Side feeder EEPROM error (optional side feeder)
0750 Document finisher EEPROM error
0970 Cleaning unit EEPROM error
1200 Duplex side registration motor error
2100 Developing motor error
2200 Drive motor error
2300 Fuser motor error
2550 Transfer motor error
3210 CIS lamp problem
3310 Optical system (AGC) problem (DP)
3500 Communication error between scanner and SHD
3900 Backup memory read/write error (scanner PWB)
3910
4120 BD initialization (C) problem
7200 Broken drum thermistor wire
7210 Shorted drum thermistor
9040 DP lift motor going up error
9050 DP lift motor going down error
9060 DP EEPROM error
9070 Communication problem between DP and SHD
9080 Communication problem between DP and CIS

Kyocera Mita 6230

Код ошибки Описание
0010 Memory PCB communication problem
0100 RAM/ROM problem
0260 Memory copy PCB 1 communication problem
0350 Mailbox communication problem
0370 Communication microcomputer problem
0380 Hard disk problem
0390 DIMM problem
1040 Optical system problem (AGC)
2100 Drive motor problem / Paper conveying motor problem
2200 Paper feed motor problem
2300 Large paper deck right lift motor problem
2310 Large paper deck left lift motor problem
2420 Upper lift motor problem
2430 Lower lift motor problem
6500 Broken fixing unit thermistor wire
7200 Broken drum thermistor wire
7210 Shorted drum thermistor
7220 Broken drum heater wire

KyoceraMita 6330/7530

Код ошибки Описание
1060 Large paper deck left lift motor problem
2550 Drive motor problem
7520 Shorted drum thermistor
7530 Broken drum thermistor wire

Ошибки финишеров

Код ошибки Описание
8010 Finisher paper conveying motor problem
8030 Finisher (upper) paper conveying belt problem
8140 Finisher tray elevation motor problem /Main tray problem
8170 Finisher front side registration motor problem
8180 Finisher rear side registration motor problem
Finisher rear jogger motor problem (для 4230/5230)
8190 Finisher trailing edge registration motor problem
8210 Finisher stapler motor problem
8220 Finisher rear stapler problem
8300 Document finisher centerfold unit communication problem
8310 Document finisher centerfold unit side registration guide problem
8320 Document finisher centerfold unit centering plate problem
8330 Document finisher centerfold blade problem

Ошибки финишеров KM-2530/3530/3035/4035/5035

Код ошибки Описание
8300 Booklet stitcher paper ejection motor problem
8310 Booklet stitcher elevation motor problem
8320 Booklet stitcher rear jog motor problem
8330 Booklet stitcher front jog motor problem
8340 Booklet stitcher staple motor problem
8350 Booklet stitcher batch processing motor problem
8360 Booklet stitcher stapler shift motor problem
8370 Booklet stitcher paddle motor problem
8380 Booklet stitcher folding problem
8390 Booklet stitcher backup RAM data problem
8400 Booklet stitcher incorrect type problem
8410 Booklet stitcher punch motor problem
8420 Booklet stitcher shift motor problem
8430 Booklet stitcher punch communication problem
8440 Booklet stitcher punch sensor problem
8450 Booklet stitcher side punch sensor problem
8460 Booklet stitcher punch backup RAM data problem
8470 Booklet stitcher punch dust sensor problem
8480 Booklet stitcher broken punch power source wire problem
8500 Mailbox drive motor problem

Ошибки финишера KM-6230

Код ошибки Описание
8180 Finisher rear jogger motor problem
8310 Booklet stitcher paper ejection motor problem
8320 Booklet stitcher elevation motor problem
8330 Booklet stitcher jog motor problem
8340 Booklet stitcher staple motor problem
8350 Booklet stitcher stapler unit shift motor problem
8360 Booklet stitcher stack level detection sensor problem
8370 Booklet stitcher punch motor problem
8380 Booklet stitcher punch shift motor problem
8390 Booklet stitcher swing motor problem
8400 Booklet stitcher backup RAM data problem
8410 Booklet stitcher punch unit backup RAM data problem
8420 Booklet stitcher positioning plate motor problem
8430 Booklet stitcher folding motor problem
8440 Booklet stitcher guide motor problem
8450 Booklet stitcher jog motor problem
8460 Booklet stitcher rear staple motor problem
8470 Booklet stitcher front staple motor problem
8480 Booklet stitcher thrust motor problem
8490 Booklet stitcher communication error

Ошибки финишеров KM-6330/7530/6030/8030

Код ошибки Описание
8000 Document finisher incorrect type problem (для 6330/7530)
8020 Finisher punch motor problem
8040 Finisher lower paper conveying belt problem
8150 Finisher multi job tray problem
8170 Front upper side-registration guide problem
8180 Finisher rear upper side-registration guide problem
8190 Finisher lower side-registration guide problem
8220 Finisher front clincher problem
8230 Finisher rear stapler problem
8240 Finisher rear clincher problem

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  1. 12-07-2020


    #1

    thinkink is offline


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    Kyocera M3550 C1010 error

    I have a customer with a Kyocera M3550 that is showing a C1010 error. I am planning on swapping out machine, due to the difficulty of this repair. However the customer does a lot of faxing, and had a number of faxes in memory due to the error. He did not have any forwarding set up so he does not have a copy of these and really needs them.
    1. Does someone know if there is a way to forward faxes waiting to print in the job log? Or if this printer will print from a second cassette or MP tray with this error? Trying to gather some info before I go out.
    thank you


  2. 12-07-2020


    #2

    Re: Kyocera M3550 C1010 error

    the code is probably intermittent, it’ll work better with fewer sheets in the cassette (less weight)

    or reboot to clear, keep the cassette out and load the bypass.

    By the way you can fix your machine by using a CT3100 cassette

    302MS93011

    It’s spring loaded so it doesn’t use the machine lift drive.


  3. 12-07-2020


    #3

    thinkink is offline


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    Re: Kyocera M3550 C1010 error

    Quote Originally Posted by JR2ALTA
    View Post

    the code is probably intermittent, it’ll work better with fewer sheets in the cassette (less weight)

    or reboot to clear, keep the cassette out and load the bypass.

    By the way you can fix your machine by using a CT3100 cassette

    302MS93011

    It’s spring loaded so it doesn’t use the machine lift drive.

    *********************************
    Thank you!


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  • Code: 0030
  • Description: FAX control PWB system error
    Processing with the fax software was disabled due to a software problem.
  • Remedy: FAX control PWB: 1. Turn the main power swtch off and after 5 seconds, re-mount the FAX controller PWB, then turn power on. 2. Reinstall the fax software. 3. Replace the FAX control PWB.
  • Code: 0070
  • Description: FAX control PWB incompatible detection error
    Abnormal detection of FAX control PWB incompatibility In the initial communication with the FAX control PWB, any normal communication command is not transmitted.
  • Remedy: FAX control PWB (The FAX PWB installed will not be the one designed for the machine.): 1. Install the FAX system designed for the model. 2. Reinstall the fax software.
  • Code: 0080
  • Description: Option printing system device error.
    The version of the FPGA for Fiery control is not readable. (Defective FPGA)
  • Remedy: Defective FPGA for printing system control.: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Replace the main PWB
  • Code: 0100
  • Description: Backup memory device error
  • Remedy: EEPROM(main PWB): 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Check that the EEPROM on the main circuit PWB is peroperly installed on the main circuit PWB and, if not, re-install it. 3. Replace the main PWB.
  • Code: 0120
  • Description: MAC address data error
    For data in which the MAC address is invalid.
  • Remedy: EEPROM(main PWB): 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Check the MAC address on the network status page. 3. If it is blank, obtain an EEPROM with its MAC address written from the service support and install. 4. Replace the main PWB.
  • Code: 0150
  • Description: Backup memory read/write error (engine PWB)
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated 5 times successively. Mismatch of reading data from 2 locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: EEPROM(Engine PWB): 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Check that the EEPROM is peroperly installed on the engine PWB and reinstall it. 3. Replace the engine PWB. 4. Check the EEPROM and if the data are currupted, contact the service support.
  • Code: 0160
  • Description: Backup memory data error (engine PWB)
    Reading data from EEPROM is abnormal.
  • Remedy: EEPROM: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Execute U021 — memory initializing 3. If the EEPROM data are currupted, contact the service support.
  • Code: 0170
  • Description: Billing counting error
    The values on the main circuit PWB and on the engine do not match for any of charging counter, life counter, and scanner counter.
  • Remedy: EEPROM: 1. Check that the EEPROMs installed in the main PWB and the engine PWB are correct and, if not, use the correct EEPROM for the model. 2. If the EEPROM data are currupted, contact the service support.
    Main PWB: Replace the main PWB.
    Engine PWB: Replace the engine PWB
  • Code: 0180
  • Description: Machine number mismatch
    Machine number of main and engine does not match.
  • Remedy: Data damage of EEPROM: 1. Confirm the machine data for the main and engine units by using U004. 2. If the serial number data of different models is alternately displayed, install the correct EEPROM in the PWB of the wrong serial number data. 3. Contact the Service Support.
  • Code: 0350
  • Description: Panel PWB communication error (electronic volume I2C communication error)
    NACK is received during I2C communication -> retried 5 times -> rebooting command sent -> retried 5 times If NACK is still received.
  • Remedy: Operation PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Operation PWB (YC10) and Main PWB (YC6) 3. If the wiring is disconnected, shorted or grounded, replace the wiring.
    Main PWB: Replace the main PWB.
  • Code: 0620
  • Description: FAX image DIMM error
    1. The Fax image DIMM has not been installed. 2. Fax image DIMM access error.
  • Remedy: FAX image DIMM: 1. Install the FAX image DIMM supplied in the FAX system onto the main PWB. 2. Firmly install the FAX image DIMM again onto the main board. 3. Check the FAX image DIMM terminals and remove any foreign objects that may be adhered to it. 4. Replace with a new FAX image DIMM.
  • Code: 0630
  • Description: DMA error
    DMA transmission of image data does not complete within the specified period of time.
  • Remedy: DP CIS: 1. Reconnect the CIS signal line. 2. Confirm that the CIS connector terminals are firmly connected. Insert the connector all the way in. 3. If the wiring is disconnected, shorted or grounded, replace the wiring.
    DP main PWB: Main PWB 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. 2. If the wiring is disconnected, shorted or grounded, replace the wiring. Wiring that connects the CIS and the DP controller PWB. Wiring that connects the DP main PWB and the main PWB. 3. Replace the DP main PWB. 4. Replace the main PWB.
  • Code: 0640
  • Description: Hard disk error
    The hard disk cannot be accessed.
  • Remedy: HDD: 1. If an abnormal noise is heard from the HDD, replace the HDD. 2. Check the SATA wiring between the HDD and the main circuit PWB for loose connection, disconnection and damages, and that it is connected into the correct terminal. Main PWB: YC1,YC27 YC2,YC32 (45/55 ppm model) 3. Replace the SATA cable. 4. Execute U024 to initialize (FULL) the HDD. 5. If an error is detected after executing U024, replace the HDD.
    Main PWB: Replace the main PWB
  • Code: 0650
  • Description: FAX image DIMM check error
    A fax image DIMM which was used with another machine is installed.
  • Remedy: FAX DIMM: 1. Confirm that a used FAX image DIMM was used instead of the FAX image DIMM contained in the FAX system. 2. If a DIMM that was used with other unit has been installed, execute maintenance mode U671 — Recovery FAX DIMM. 3. Check whether the Fax DIMM is properly inserted into the socket on the main PWB. 4. Replace with a new FAX image DIMM.
    Main PWB: Replace the main PWB.
  • Code: 0660
  • Description: Hard disk encryption key error
  • Remedy: EEPROM: 1. Execute U004 if this occurs after the EEPROM has been changed.
    HDD: 1. If an abnormal noise is heard from the HDD, replace the HDD. 2. Check the SATA wiring between the HDD and the main circuit PWB for loose connection, disconnection and damages, and that it is connected into the correct terminal. Main PWB: YC1,YC27 YC2,YC32 (45/55 ppm model) 3. Replace the SATA cable. 4. Execute U024 to initialize (FULL) the HDD. 5. If an error is detected after executing U024, replace the HDD.
    Main PWB: Replace the main PWB
  • Code: 0670
  • Description: Hard disk overwriting erasure error
  • Remedy: HDD: 1. If an abnormal noise is heard from the HDD, replace the HDD. 2. Check the SATA wiring between the HDD and the main circuit PWB for loose connection, disconnection and damages, and that it is connected into the correct terminal. Main PWB: YC1,YC27 YC2,YC32 (45/55 ppm model) 3. Replace the SATA cable. 4. Execute U024 to initialize (FULL) the HDD. 5. If an error is detected after executing U024, replace the HDD.
    Main PWB: Replace the main PWB.
  • Code: 0800
  • Description: Image processing error
    JAM010X is detected twice.
  • Remedy: Main PWB: Replace the main PWB
  • Code: 0830
  • Description: FAX control PWB flash program area checksum error
    A checksum error occurred with the program of the FAX control PWB.
  • Remedy: FAX software: 1. Reinstall the fax software.
    FAX control PWB: 1. Execute initializing by U600. 2. Replace the FAX control PWB.
  • Code: 0840
  • Description: Faults of RTC
    (“Time for maintenance T” is displayed) [Check at power up] The RTC setting has reverted to a previous state. The machine has not been powered for 5 years (compared to the settings stored periodically in the EEPROM). The RTC setting is older than 00:01 on January 1, 2000. [Checked periodically (in 5- minute interval) after powered up] The RTC setting has reverted to a state older than the last time it was checked. 10 minutes have been passed since the previous check. After C840 is detected, the machine enters in disconnection mode after the main power switch has been switched on and off and indicates ‘Maintenance T.’
  • Remedy: Battery ( main PWB): 1. Make sure that the back-up batteries on the main PWB are not short-circuited. 2. Reset Maintenance T by executing U906 . 3. If the same C call is displayed when power is switched on and off, replace the back up battery. 4. If communication error (due to a noise, etc.) is present with the RTC on the main circuit PWB, check the PWB is properly grounded.
    Main PWB: Replace the main PWB
  • Code: 0870
  • Description: PCFAX control PWB to main PWB high capacity data transfer error
    High-capacity data transfer between the FAX control PWB and the main PWB of the machine was not normally performed even if the data transfer was retried the specified times.
  • Remedy: FAX control PWB: 1. Turn the main power swtch off and after 5 seconds, re-mount the FAX controller PWB, then turn power on. 2. Replace the FAX control PWB.
    HDD: Execute U024 to initialize the HDD.
    Main PWB: Replace the main PWB
  • Code: 0920
  • Description: Fax file system error
    The backup data is not retained for file system abnormality of flash memory of the FAX control PWB.
  • Remedy: FAX control PWB: 1. Execute initializing by U600 (Refer to the FAX service manual). 2. Replace the FAX control PWB.
  • Code: 0980
  • Description: 24 V power down detect
    If a 24V power disconnection signal is observed and a 12V power disconnection signal is observed simultaneously for one second.
  • Remedy: Power source PWB: 1. Check the +24V output is given at YC12- 1 to 3 of the power circuit PWB. 2. Replace the power source PWB
  • Code: 1000
  • Description: MP lift motor error
    If the MP lift sensor 1 (upper limit detect) or 2 (bottom detect) is not detectable to be turned on while the MP lift motor is ascending or descending.
  • Remedy: Manual feed lift base elevating mechanism: 1. Check that the paper lift base of the manual feed tray can smoothly ascend and descent, if not, repair or replace. 2. Check that the lift lever is located so that it can ascend or descend by the lift motor cam and that it not damaged and, if necessary, re-install or replace the manual feed table.
    MP lift motor: 1. Check that the paper elevator has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MP lift motor and Relay PWB (YC3) Relay PWB (YC12) and Feed PWB1 (YC17) Feed PWB1 (YC1) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the MP lift motor.
    MP lift sensor1 MP lift sensor2: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MP lift sensor1,2 and Relay PWB (YC3) Relay PWB (YC12) and Feed PWB1(YC17) Feed PWB1 (YC1) and Engine PWB (YC6) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the MP lift sensor1 or MP lift sensor2.
    Feed PWB 2: Replace the Feed PWB 2.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 1010
  • Description: Lift motor 1 error
    After cassette 1 is inserted, lift sensor 1 does not turn on within 12 s. This error is detected 5 times successively. The lock signal of the motor is detected continuously for 1 s. This error is detected 5 times successively.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    Lift motor 1: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Lift motor 1 and Feed PWB 2 (YC3) Feed PWB 2 (YC1) and Engine PWB (YC4) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the lift motor 1.
    Lift sensor 1: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Lift sensor 1 and Feed PWB 2 (YC8) Feed PWB 2 (YC1) and Engine PWB (YC4) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the lift sensor1.
    Feed PWB 2: Replace the Feed PWB 2.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 1020
  • Description: Lift motor 2 error
    After cassette 2 is inserted, lift sensor 2 does not turn on within 12 s. This error is detected 5 times successively. The lock signal of the motor is detected continuously for 1 s. This error is detected 5 times successively.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    Lift motor 2: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Lift motor 2 and Feed PWB 2 (YC3) Feed PWB 2 (YC1) and Engine PWB (YC4) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the lift motor 2.
    Lift sensor 2: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Lift sensor 2 and Feed PWB 2 (YC8) Feed PWB 2 (YC1) and Engine PWB (YC4) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the lift sensor2.
    Feed PWB 2: Replace the Feed PWB 2.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 1030
  • Description: PF lift motor 1 error (paper feeder)
    After cassette 3 is inserted, PF lift sensor 1 does not turn on within 12 s. This error is detected 5 times successively. During driving the motor, the lift overcurrent protective monitor signal is detected for 1 s or more 5 times successively. However, the first 1 s after motor is turned on is excluded from detection.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    PF Lift motor 1: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift motor 1 and main PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. PFReplace the lift motor 1.
    PF Lift sensor 1: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift sensor 1 and PF main PWB (YC7) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the lift sensor 1.
    PF main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1040
  • Description: PF lift motor 2 error (paper feeder)
    After cassette 4 is inserted, PF lift sensor 2 does not turn on within 12 s. This error is detected 5 times successively. During driving the motor, the lift overcurrent protective monitor signal is detected for 1 s or more 5 times successively. However, the first 1 s after motor is turned on is excluded from detection.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    PF Lift motor 2: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift motor 2 and PF main PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the PF Lift motor2.
    PF Lift sensor 2: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift sensor 2 and PF main PWB (YC7) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the PF Lift sensor 2.
    PF main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1050
  • Description: SM lift motor error (side multi tray)
    [45 ppm/55 ppm model] After cassette 5 is inserted, SM lift sensor does not turn on within 12 s. This error is detected 5 times successively. (Time to detect is 2 seconds at the second time and later.) During driving the motor, the lift overcurrent protective monitor signal is detected for 1 s or more 5 times successively. However, the first 1 s after motor is turned on is excluded from detection.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    SM Lift motor: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM Lift motor and SM main PWB (YC5) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the SM Lift motor.
    SM Lift sensor: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM Lift sensor and SM main PWB (YC7) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the SM Lift sensor.
    SM main PWB: Replace the SM main PWB (Refer to the service manual for the paper feeder).
  • Code: 1060
  • Description: PF lift motor 1 error (side paper feeder)
    [45 ppm/55 ppm model] After cassette 6 is inserted, PF lift sensor 1 does not turn on within 12 s. This error is detected 5 times successively. (Time to detect is 2 seconds at the second time and later.) During driving the motor, the lift overcurrent protective monitor signal is detected for 1 s or more 5 times successively. However, the first 1 s after motor is turned on is excluded from detection. *:The lift over-current protection monitor signal has been detected for 200ms or longer where LFC is installed.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace. PF Lift motor 1: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift motor 1 and PF main PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the lift motor 1.
    PF Lift sensor 1: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift sensor1 and PF main PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the lift sensor 1.
    PF main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1070
  • Description: PF lift motor 2 error (side paper feeder)
    [45 ppm/55 ppm model] After cassette 7 is inserted, PF lift sensor 2 does not turn on within 12 s. This error is detected 5 times successively. (Time to detect is 2 seconds at the second time and later.) During driving the motor, the lift overcurrent protective monitor signal is detected for 1 s or more 5 times successively. However, the first 1 s after motor is turned on is excluded from detection. *:The lift over-current protection monitor signal has been detected for 200ms or longer where LFC is installed.
  • Remedy: Cassette lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    PF Lift motor2: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift motor 2 and PF main PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the PF Lift motor2
    PF Lift sensor2: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift sensor 2 and PF main PWB (YC4) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. PFReplace the lift sensor2.
    PF main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1100
  • Description: PF lift motor 1 error (large capacity feeder)
    After cassette 3 is inserted, PF lift sensor 1 does not turn on within 23 s. This error is detected 5 times successively. (Time to detect is 2 seconds at the second time and later.) During driving the motor, the lift overcurrent protective monitor signal is detected for 200 ms or more 5 times successively. However, the first 1 s after PF lift motor 1 is turned on is excluded from detection.
  • Remedy: Paper feeder lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    PF Lift motor1: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift motor 1 and PF main PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the PF lift motor1.
    PF Lift sensor1: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift sensor 1 and PF main PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the PF lift sensor1.
    PF main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1110
  • Description: PF lift motor 2 error (large capacity feeder)
    After cassette 4 is inserted, PF lift sensor 2 does not turn on within 23 s. This error is detected 5 times successively. (Time to detect is 2 seconds at the second time and later.) During driving the motor, the lift overcurrent protective monitor signal is detected for 200 ms or more 5 times successively. However, the first 1 s after PF lift motor 2 is turned on is excluded from detection.
  • Remedy: Paper feeder lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    PF Lift motor 2: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift motor 2 and PF main PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the PF Lift motor2.
    PF Lift sensor2: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF Lift sensor 2 and PF main PWB (YC4) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the PF Lift sensor 2.
    PF main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1140
  • Description: SD lift motor error (side deck)
    After cassette 5 is inserted, SD lift sensor does not turn on within 30 s. The lock signal of the motor is detected continuously for 200 ms.
  • Remedy: Paper feeder lift base elevating mechanism: Check that the cassette base can be manipulated smoothly, if not, repair or replace.
    SD Lift motor: 1. Check that the cassette base has been ascended. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SD Lift motor and SD main PWB (YC8) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the SD Lift motor.
    SD Lift sensor: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SD Lift sensor and SD main PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the SD Lift sensor.
    SD main PWB: Replace the SD main PWB (Refer to the service manual for the paper feeder).
  • Code: 1250
  • Description: SM multi feed sensor communication error (side multi tray)
    [45 ppm/55 ppm model] A communication error is detected 3 times in succession.
  • Remedy: Side multi tray: Check the wiring connection status with the main unit and, if necessary, try connecting it again.
    SM main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM main PWB (YC1) and Engine PWB (YC19) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the SM main PWB (Refer to the service manual for the paper feeder).
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB .
  • Code: 1350
  • Description: SM multi feed sensor error (side multi tray)
    [45 ppm/55 ppm model] The SM multi feed sensor has detected multi feeding 5 times successively.
  • Remedy: SM multi feed sensor: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM multi feed sensor and SM main PWB (YC11) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the SM multi feed sensor.
    SM main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1400
  • Description: Rotary guide motor error
    The guide sensor is not detected to be on at the home position detection with the rotary guide for three times in a row.
  • Remedy: Rotary guide motor: 1. Check the rotary guide and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Rotary guide motor and BR PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the rotary guide motor.
    BR PWB: Replace the BR PWB.
  • Code: 1410
  • Description: Rotary de-curler error
    If the de-curler won’t turn On/ Off despite it has been activated for 400 steps during waiting for the de-curler sensor to be On/Off three times in a row.
  • Remedy: Rotary de-curler motor: 1. Check the rotary de-curler and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Rotary de-curler motor and BR PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the rotary de-curler motor.
    BR PWB: Replace the BR PWB.
  • Code: 1450
  • Description: SM multi feed sensor backup error (side multi tray)
    [45 ppm/55 ppm model] When writing the data, read and write data does not match 3 times in succession. Deleting a block has failed three times in a row. Writing won’t complete in 200 ms after writing has commenced.
  • Remedy: SM multi feed sensor: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM multi feed sensor and SM main PWB (YC11) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the SM multi feed sensor.
    SM main PWB: Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1710
  • Description: Side multi tray incompatible detection error
    [30 ppm/35 ppm model] The side multi tray has been installed with a device to which it is incompatible.
  • Remedy: The side multi tray is installed with a device to which it is incompatible: Install the side multi-tray with the target model.
  • Code: 1800
  • Description: Paper feeder communication error
    A communication error from paper feeder is detected 10 times in succession.
  • Remedy: Paper feeder: Check the wiring connection status with the main unit and, if necessary, try connecting it again.
    PF main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF main PWB (YC13) and Engine PWB (YC19) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the PF main PWB (Refer to the service manual for the paper feeder).
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 1810
  • Description: Side multi tray communication error
    [45 ppm/55 ppm model] A communication error from side multi tray is detected 10 times in succession.
  • Remedy: Side multi tray: Check the wiring connection status with the main unit and, if necessary, try connecting it again.
    SM main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM main PWB (YC1) and Engine PWB (YC19) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the SM main PWB (Refer to the service manual for the paper feeder).
    Engine PWB: Check the engine software and upgrade to the latest, if necessary. Replace the engine PWB.
    SM main PWB: Replace the SM main PWB (Refer to the service manual for the paper feeder).
  • Code: 1820
  • Description: Side paper feeder communication error
    [45 ppm/55 ppm model] A communication error from paper feeder is detected 10 times in succession.
  • Remedy: Side paper feeder: Check the wiring connection status with the main unit and, if necessary, try connecting it again.
    SM main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM main PWB (YC1) and Engine PWB (YC19) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the SM main PWB (Refer to the service manual for the paper feeder).
    PF main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF main PWB (YC13) and SM main PWB (YC4) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the PF main PWB (Refer to the service manual for the paper feeder).
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 1900
  • Description: Paper feeder EEPROM error
    When writing the data, read and write data does not match 3 times in succession.
  • Remedy: PF main PWB (EEPROM): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. 2. Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1910
  • Description: Side multi tray EEPROM error
    [45 ppm/55 ppm model] When writing the data, read and write data does not match 3 times in succession.
  • Remedy: SM main PWB (EEPROM): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. 2. Replace the SM main PWB (Refer to the service manual for the paper feeder).
  • Code: 1920
  • Description: Side paper feeder EEPROM error
    [45 ppm/55 ppm model] When writing the data, read and write data does not match 3 times in succession.
  • Remedy: PF main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. 2. Replace the PF main PWB (Refer to the service manual for the paper feeder).
  • Code: 1950
  • Description: Intermediate transfer belt unit EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated 5 times successively. Mismatch of reading data from 2 locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: Transfer belt sensor: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Engine PWB (YC27) and RFID PWB (4P connector) (Check wirings on the RFID side since the signal line for the intermediate transfer belt sensor EEPROM on the engine PWB and the signal line for the toner container RFID are the same.) Intermediate transfer belt unit and Engine PWB (YC3) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Intermediate transfer belt unit.
  • Code: 2101
  • Description: Developer motor K error
    After developer motor K is driven, the ready signal does not turn to L within 5 s. After developer motor K is stabilized, the ready signal is at the H level for 5 s continuously.
  • Remedy: Developer unit K: 1. Check that the developer waste lock has been released and, if not, release the lock . 2. Check that the gears and spiral screw of the developer unit are not damaged. 3. Confirm that the developer roller can rotate. 4. If it won’t rotate, replace the developer unit.
    Developer motor K: 1. To check the motor operation, execute DLP(K) by U030 . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer motor K and Motor control PWB (YC7) Motor control PWB (YC3) and Engine PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Developer motor K.
    Motor control PWB: Replace the Motor control PWB
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2103
  • Description: Developer motor MCY error
    After developer motor MCY is driven, the ready signal does not turn to L within 5 s. After developer motor MCY is stabilized, the ready signal is at the H level for 5 s continuously.
  • Remedy: Developer unit MCY: 1. Check that the developer waste lock has been released and, if not, release the lock . 2. Check that the gears and spiral screw of the developer unit are not damaged. 3. Confirm that the developer roller can rotate. 4. If it won’t rotate, replace the developer unit.
    Developer motor MCY: 1. To check the motor operation, execute DLP(MCY) by U030 . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer motor MCY and Motor control PWB (YC7) Motor control PWB (YC3) and Engine PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Developer motor MCY.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2201
  • Description: Drum motor K steady-state error
    After drum motor K is stabilized, the ready signal is at the H level for 5 s continuously.
  • Remedy: Drum unit: 1. Execute U030 Belt Meand (transfer Motor) and check that the drum motor can rotate. 2. Confirm that the drum or the drum screw can rotate. 3. If it won’t rotate, replace the drum unit.
    Drum motor K: 1. To check the motor operation, execute U030 Belt Meand (transfer motor). 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor K and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the drum motor K.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2202
  • Description: Drum motor C steady-state error
    [45 ppm/55 ppm model] After drum motor C is stabilized, the ready signal is at the H level for 5 s continuously.
  • Remedy: Drum unit: 1. Execute U030 Belt Meand (transfer Motor) and check that the drum motor can rotate. 2. Confirm that the drum or the drum screw can rotate. 3. If it won’t rotate, replace the drum unit.
    Drum motor C: 1. To check the motor operation, execute U030 Belt Meand (transfer motor) . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor C and Motor control PWB (YC4) Motor control PWB (YC3) and Engine PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Drum motor C.
    Motor control PWB: Replace the Motor control PWB
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2203
  • Description: Drum motor MCY steadystate error
    [30 ppm/35 ppm model] After drum motor MCY is stabilized, the ready signal is at the H level for 5 s continuously.
  • Remedy: Drum unit: 1. Execute U030 Belt Meand (transfer Motor) and check that the drum motor can rotate . 2. Confirm that the drum or the drum screw can rotate. 3. If it won’t rotate, replace the drum unit.
    Drum motor MCY: 1. To check the motor operation, execute U030 Belt Meand (transfer motor) . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor MCY and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Drum motor MCY.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2203
  • Description: Drum motor M steady-state error
    [45 ppm/55 ppm model] After drum motor M is stabilized, the ready signal is at the H level for 5 s continuously.
  • Remedy: Drum unit: 1. To check the motor operation, execute U030 Belt Meand (transfer motor). . 2. Decrease Vpp using U100. Change “set ac gain” of U100 from Auto to mode1. 3. Confirm that the drum or the drum screw can rotate. 4. If it won’t rotate, replace the drum unit.
    Drum motor M: 1. To check the motor operation, execute U030 Belt Meand (transfer motor) . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. 3. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. Drum motor M and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Drum motor MCY.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2211
  • Description: Drum motor K startup error
    Drum motor K is not stabilized within 5 s since the motor is activated.
  • Remedy: Drum unit: 1. To check the motor operation, execute U030 Belt Meand (transfer motor). . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Decrease Vpp using U100. Change “set ac gain” of U100 from Auto to mode1. 4. Confirm that the drum or the drum screw can rotate. 5. If it won’t rotate, replace the drum unit.
    Drum motor K: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor K and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum motor K.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2212
  • Description: Drum motor C startup error
    [45 ppm/55 ppm model] Drum motor C is not stabilized within 5 s since the motor is activated.
  • Remedy: Drum unit: 1. To check the motor operation, execute U030 Belt Meand (transfer motor). 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Decrease Vpp using U100. Change “set ac gain” of U100 from Auto to mode1. 4. Confirm that the drum or the drum screw can rotate. 5. If it won’t rotate, replace the drum unit.
    Drum motor C: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor C and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum motor C.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 2213
  • Description: Drum motor MCY startup error
    [30 ppm/35 ppm model] Drum motor MCY is not stabilized within 5 s since the motor is activated.
  • Remedy: Drum unit: 1. To check the motor operation, execute U030 Belt Meand (transfer motor). . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Decrease Vpp using U100. Change “set ac gain” of U100 from Auto to mode1. 4. Confirm that the drum or the drum screw can rotate. 5. If it won’t rotate, replace the drum unit.
    Drum motor MCY: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor MCY and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum motor MCY.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2213
  • Description: Drum motor M startup error
    [45 ppm/55 ppm model] Drum motor M is not stabilized within 5 s since the motor is activated.
  • Remedy: Drum unit: 1. To check the motor operation, execute Belt Mean (transfer motor) by U030 motor operation check. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Decrease Vpp using U100. Change set ac gain of U100 from Auto to mode1. 4. Confirm that the drum or the drum screw can rotate. 5. If it won’t rotate, replace the drum unit.
    Drum motor M: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Drum motor M and Motor control PWB (YC5) Motor control PWB (YC3) and Engine PWB (YC9) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum motor MCY.
    Motor control PWB: Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2300
  • Description: Fuser motor error
    After fuser motor is driven, the ready signal does not turn to L within 2 s. After fuser motor is stabilized, the ready signal is at the H level for 1 s continuously.
  • Remedy: Fuser motor: 1. To check the motor operation, execute U030 Fuser (fuser motor). 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser motor and Feed PWB 1(YC18) Feed PWB 1(YC1) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the fuser motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Feed PWB 1: Replace the Feed PWB 1.
    Fuser unit: Replace the fuser unit.
  • Code: 2500
  • Description: Paper feed motor error
    After paper feed motor is driven, the ready signal does not turn to L within 2 s. After paper feed motor is stabilized, the ready signal is at the H level for 1 s continuously.
  • Remedy: Paper feed motor: 1. To check the motor operation, execute U030 Feed (paper feed motor). 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Paper feed motor and Feed PWB 2(YC2) Feed PWB 2(YC1) and Engine PWB (YC4) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the paper feed motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2600
  • Description: PF paper feed motor error (large capacity feeder)
    After PF paper feed motor is driven, the ready signal does not turn to L within 2 s.
  • Remedy: PF paper feed motor: 1. To check the feed unit operation, execute U247 LCF- Motor ON . 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF paper feed motor and PF main PWB (YC16) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the paper feed motor.
    PF main PWB: Replace the PF main PWB
  • Code: 2610
  • Description: PF paper feed motor error (paper feeder)
    [45 ppm/55 ppm model] After PF paper feed motor is driven, the ready signal does not turn to L within 2 s.
  • Remedy: PF paper feed motor: 1. To check the feed unit operation, execute U247 2PF — Motor ON . 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF paper feed motor and PF main PWB (YC16) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the paper feed motor.
    PF main PWB: Replace the PF main PWB
  • Code: 2640
  • Description: SD paper feed motor error (side deck)
    [45 ppm/55 ppm model] After SD paper feed motor is driven, the ready signal does not turn to L within 2 s.
  • Remedy: SD paper feed motor: 1. To check the feed unit operation, execute U247 Side deck- Motor ON . 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SD paper feed motor and SD main PWB (YC16) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the SD paper feed motor.
    SD main PWB: Replace the SD main PWB
  • Code: 2650
  • Description: SM paper feed motor error (side multi tray)
    [45 ppm/55 ppm model] After SM paper feed motor is driven, the ready signal does not turn to L within 2 s.
  • Remedy: SM paper feed motor: 1. To check the feed unit operation, execute U247 SMT- Motor ON. 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. SM paper feed motor and SM main PWB (YC5) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the SM paper feed motor.
    SM main PWB: Replace the SM main PWB
  • Code: 2660
  • Description: PF paper feed motor error (side large capacity feeder)
    [45 ppm/55 ppm model] After PF paper feed motor is driven, the ready signal does not turn to L within 2 s.
  • Remedy: PF paper feed motor: 1. To check the feed unit operation, execute U247 Side LCF — Motor ON. 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF paper feed motor and PF main PWB (YC16) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the PF paper feed motor.
    PF main PWB: Replace the PF main PWB
  • Code: 2670
  • Description: PF paper feed motor error (side paper feeder)
    [45 ppm/55 ppm model] After PF paper feed motor is driven, the ready signal does not turn to L within 2 s.
  • Remedy: PF paper feed motor: 1. Execute Side 2PF — Motor ON of U247 feed unit operation check. 2. Check the paper feed roller and drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. PF paper feed motor and PF main PWB (YC16) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the PF paper feed motor.
    PF main PWB: Replace the PF main PWB
  • Code: 2700
  • Description: 3-color release motor error
    When the color release motor is driven, the color release sensor does not turn on/off for 5 s.
  • Remedy: Color release motor Color release sensor (Intermediate transfer belt unit): 1. To check the motor operation, execute U30 CMY Release. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Intermediate transfer belt unit and Engine PWB (YC3) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Intermediate transfer belt unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2730
  • Description: Secondary transfer release motor error
    When the transfer release motor is driven, the transfer release sensor does not turn on/off for 5 s.
  • Remedy: Transfer release motor: 1. To check the motor operation, execute U030 Press Release. 2. Check for broken drive gears and replace if any. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Transfer release motor and relay PWB (YC14) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Transfer release motor.
    Transfer release sensor: 1. When abnormal noise is observed at the execution of Press Release of U030 motor operation check. 2. Check that the sensor and its mounting board are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. 4. Replace the Transfer release motor.
    Paper conveying unit: 1. The main-unit access drawer of the paper conveying unit has no foreign objects adhered or no distorted pins and, if necessary, repair. 2. Check the paper conveying unit is firmly closed. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Relay PWB (YC1) and Feed PWB 1(YC14) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the paper conveying unit and execute U052.
    Feed PWB 1: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Feed PWB 1 (YC1) and Engine PWB (YC6) 2. Check that the IC on the feed circuit PWB1 is not damaged (by an overcurrent or foreign object) and, if necessary, replace.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2760
  • Description: Transfer motor startup error
    Transfer motor is not stabilized within 5 s since the motor is activated.
  • Remedy: Transfer motor: 1. To check the motor operation, execute U030 Belt Meand. 2. Rotate the drive gear, the belt and the roller by the hand and check that they are not unusually loaded. 3. Clean the Intermediate transfer belt unit. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Transfer motor and Feed PWB 1 (YC13) Feed PWB 1(YC2) and Engine PWB (YC5) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the Transfer motor.
    Feed PWB 1: Replace the Feed PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2770
  • Description: Intermediate transfer belt meandering correction error
    If the intermediate transfer belt position detecting sensor has derived an incorrect value.
  • Remedy: Intermediate transfer belt unit: 1. Check that the Intermediate transfer belt unit has been properly installed so that the intermediate belt unit waste toner shutter won’t be derailed when the belt unit is strongly inserted. 2. Reinstall the intermediate transfer belt unit.(Insert slowly all the way in. 3. Run U468 Belt Position with B/W and confirm “ angle” (position of belt) is within the range (6 to 26). 4. Check that the main unit is placed perfectly horizontal. 5. Replace the intermediate transfer belt unit.
    Transfer belt sensor (Intermediate transfer belt unit): 1. Clean the toner off of the sensor and its proximity using a blower. 2. Check the sensor actuator are correctly positioned.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2780
  • Description: Intermediate transfer belt skew correction sensor error
    An abnormal value is detected to transfer skew sensor.
  • Remedy: Transfer belt skew sensor (Intermediate transfer belt unit): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. intermediate transfer belt unit and Engine PWB (YC3) 1. Replace the intermediate transfer belt unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 2790
  • Description: Intermediate transfer belt skew correction motor error
    When the transfer skew motor is driven, timeouts (300 ms) were detected twice in a row.
  • Remedy: Transfer belt skew motor: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. intermediate transfer belt unit and Engine PWB (YC3) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the intermediate transfer belt unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 2810
  • Description: Inner waste toner motor error
    Initialized when an error is constantly observed for 2 seconds after the inner waste tonner motor is activated. An error is detected twice for 2.5 seconds after rebooting. The lock detect signal won’t be H level three times in a row within 200 ms at 1.25 ms cycles after the inner waste tonner motor has been driven.
  • Remedy: Waste toner box: 1. Rotate the waste toner spiral by the hand and check that they are not unusually loaded. 2. If the spiral won’t rotate, replace the waste toner tank.
    Waste toner motor: 1. Rotate the drive gear by the hand and check that they are not unusually loaded. 2. Clean the drive gears and the axle holder. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Waste toner motor and Front PWB (YC16) Front PWB (YC3) and Engine PWB (YC7) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the waste toner motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2820
  • Description: Intermediate transfer belt motor steady-state error
    After transfer motor is stabilized, the ready signal is at the H level for 5 s continuously. The counter value obtained by timer capture is lower than 2200 for 10 times in a row.
  • Remedy: Transfer motor: 1. To check the motor operation, execute U030 Belt Meand. 2. Rotate the roller, driving gear by the hand and check that they are not unusually loaded. 3. Clean the intermediate transfer belt unit. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Transfer motor and Feed PWB 1(YC13) Feed PWB 1(YC2) and Engine PWB (YC5) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the Transfer motor.
    Feed PWB 1: Replace the Feed PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2840
  • Description: Intermediate transfer belt cleaning motor error
    After transfer cleaning motor is driven, the ready signal won’t be L lebel within 2 s. After transfer cleaning motor is stabilized, the ready signal is at the H level for 1 s continuously.
  • Remedy: Transfer cleaning motor: 1. Rotate the roller and the drive gear by the hand and check that they are not unusually loaded. 2. Check if the waste toner is remaining inside the cleaning unit without being disposed of. 3. Clean inside the cleaning unit. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Transfer cleaning motor and Engine PWB (YC3) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the transfer cleaning motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 2850
  • Description: Intermediate transferbelt sensor error
    The signal is not received for 100 ms in succession.
  • Remedy: Transfer motor: 1. To check the motor operation, execute U030 Belt Meand. 2. Rotate the roller, driving gear by the hand and check that they are not unusually loaded. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Transfer motor and Feed PWB 1(YC13) Feed PWB 1(YC1) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Transfer motor.
    Feed PWB 1: Replace the Feed PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2860
  • Description: Intermediate transfer belt sub sensor error
    The signal is not received for 100 ms in succession.
  • Remedy: Transfer belt sensor: 1. To check the motor operation, execute U030 Belt Meand. 2. Check that the drive roller for the sensor pulse can be rotated. 3. Check that the sensor is correctly positioned. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Transfer belt sensor and intermediate transfer belt unit and Engine PWB (YC3) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the intermediate transfer belt unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 2950
  • Description: Motor control PWB communication error
    A communication error from the motor control PWB is detected 10 times in succession.
  • Remedy: Motor control PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Motor control PWB (YC3) and Engine PWB (YC9) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Motor control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 3100
  • Description: Scanner carriage error
    The home position is not correct when the power is turned on, at the end of a reading process of the table and document processor.
  • Remedy: The scanner mirror frame is being locked after setup: Check whether the scanner mirror frame has been unlocked and unlock if necessary
    Scanner motor: 1. To check the scanner motor, execute U073 . 2. Move the scanner by the hand to check whether it is unusually difficult to move. 3. Check that the optical wire rope is not disengaged and engage the wire. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Scanner motor and ISC PWB (YC5) ISC PWB (YC3) and Main PWB (YC11) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the scanner motor.
    Home position sensor: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Home position sensor and ISC PWB (YC8) 3. Replace the home position sensor.
    ISC PWB: Replace the ISC PWB and execute U411
    Main PWB: Replace the main PWB
  • Code: 3210
  • Description: CIS lamp error
    When input value at the time of CIS illumination does not exceed the threshold value between 5 s
  • Remedy: CIS: 1. Execute U906 Separating Operation Release . 2. Execute CCD of U061 lamp check. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CIS and DPSHD PWB (YC2) DPSHD PWB (YC3) and DP relay PWB (YC2) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the CIS and execute U091 and U411.
    DPSHD PWB: Replace the DPSHD PWB.
    DP relay PWB: Replace the DP relay PWB.
  • Code: 3220
  • Description: CCD lamp activation error
    The threshold is calculated for colors at initialization and the pixel which does not exceed that value is greater than 1000.
  • Remedy: CIS 1. Execute U906 Separating Operation Release. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. LED lamp PWB and ISC PWB (YC6) CCD PWB (YC2) and ISC PWB (YC9) ISC PWB (YC3) and Main PWB (YC11) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. If the LED lamp won’t light, replace the LED PWB and execut U411.
    ISC PWB: Replace the ISC PWB and execute U411.
    Main PWB: Replace the main PWB
  • Code: 3300
  • Description: Optical system (AGC) error
    One of the gains is FF or 0x89 during the CCD lamp AGC is being processed.
  • Remedy: LED lamp PWB: 1. To check the lamp, execute U061 CCD. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. LED lamp PWB and ISC PWB (YC6) CCD PWB (YC2) and ISC PWB (YC9) ISC PWB (YC3) and Main PWB (YC11) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. If the LED lamp won’t light, replace the LED PWB and execut U411.
    CCD PWB: Replace the ISU and execute U411
    ISC PWB: Replace the ISC PWB and execute U411.
    Main PWB: Replace the main PWB.
  • Code: 3310
  • Description: CIS AGC error
    After AGC, correct input is not obtained at CIS.
  • Remedy: CIS: 1. Execute U906 Separating Operation Release. 2. To check the lamp, execute U061 CCD. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP CIS and DPSHD PWB (YC2) DPSHD PWB (YC3) and DP relay PWB (YC2) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the CIS and execute U091 and U411.
    DPSHD PWB: Replace the DPSHD PWB.
  • Code: 3500
  • Description: Communication error between scanner and ASIC
    An error code is detected.
  • Remedy: ISC PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. ISC PWB (YC3) and Main PWB (YC11) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the ISC PWB and execute U411.
    Main PWB Replace the main PWB.
  • Code: 3600
  • Description: Scanner sequence error
  • Remedy: ISC PWB: 1. Execute U021 memory initializing. 2. Replace the ISC PWB and execute U411.
  • Code: 3700
  • Description: Scanner device error
  • Remedy: CCD (ISU): Since the ISU is mounted with a CCD of different type, install the ISU that matches with the model.
  • Code: 3800
  • Description: AFE error
    When writing the data, read and write data does not match 3 times in succession. No response is received in 100 ms from AEF.
  • Remedy: ISC PWB: 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. CCD PWB (YC2) and ISC PWB (YC9) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the ISC PWB and execute U411.
    CCD PWB: Replace the ISU PWB and execute U411.
  • Code: 3900
  • Description: Backup memory read/write error (ISC PWB)
    Read and write data does not match.
  • Remedy: Backup memory (ISC PWB): 1. Turn the main power switch off and after 5 seconds, turn it on. 2. Replace the ISC PWB and execute U411.
  • Code: 4001
  • Description: Polygon motor K synchronization error
    After polygon motor K is driven, the ready signal does not turn to L within 30 s. The polygon motor speed won’t stabilize within 10 s.
  • Remedy: Polygon motor K (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor K and LSU relay PWB (YC4) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4002
  • Description: Polygon motor C synchronization error
    After polygon motor C is driven, the ready signal does not turn to L within 30 s. The polygon motor speed won’t stabilize within 10 s.
  • Remedy: Polygon motor C (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor C and LSU relay PWB (YC9) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4003
  • Description: Polygon motor M synchronization error
    After polygon motor M is driven, the ready signal does not turn to L within 30 s. The polygon motor speed won’t stabilize within 10 s.
  • Remedy: Polygon motor M (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor M and LSU relay PWB (YC7) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4004
  • Description: Polygon motor Y synchronization error
    After polygon motor Y is driven, the ready signal does not turn to L within 30 s. The polygon motor speed won’t stabilize within 10 s.
  • Remedy: Polygon motor Y (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor Y and LSU relay PWB (YC11) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4011
  • Description: Polygon motor K steadystate error
    After polygon motor K is stabilized, the ready signal is at the H level for 15 s continuously.
  • Remedy: Polygon motor K (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor K and LSU relay PWB (YC4) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4012
  • Description: Polygon motor C steadystate error
    After polygon motor C is stabilized, the ready signal is at the H level for 15 s continuously.
  • Remedy: Polygon motor C (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor C and LSU relay PWB (YC9) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4013
  • Description: Polygon motor M steadystate error
    After polygon motor M is stabilized, the ready signal is at the H level for 15 s continuously.
  • Remedy: Polygon motor M (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor M and LSU relay PWB (YC7) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: Check the engine software and upgrade to the latest, if necessary. Replace the engine PWB
  • Code: 4014
  • Description: Polygon motor Y steadystate error
    After polygon motor Y is stabilized, the ready signal is at the H level for 15 s continuously.
  • Remedy: Polygon motor Y (LSU): 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Polygon motor Y and LSU relay PWB (YC11) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4101
  • Description: BD initialization error K
    After polygon motor K is driven, the BD signal is not detected for 1 s.
  • Remedy: PD PWB K (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC5) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4102
  • Description: BD initialization error C
    After polygon motor C is driven, the BD signal is not detected for 1 s.
  • Remedy: PD PWB C (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC10) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 4103
  • Description: BD initialization error M
    After polygon motor M is driven, the BD signal is not detected for 1 s.
  • Remedy: PD PWB M (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC8) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4104
  • Description: BD initialization error Y
    After polygon motor Y is driven, the BD signal is not detected for 1 s.
  • Remedy: PD PWB Y (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC12) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4201
  • Description: BD steady-state error K
    The BD signal is not detected.
  • Remedy: PD PWB K (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC5) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, shorted or grounded, replace the FCC wiring. 3. Replace the laser scanner unit. Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 4202
  • Description: BD steady-state error C
    The BD signal is not detected.
  • Remedy: PD PWB C (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC10) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4203
  • Description: BD steady-state error M
    The BD signal is not detected.
  • Remedy: PD PWB M (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC8) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 4204
  • Description: BD steady-state error Y
    The BD signal is not detected.
  • Remedy: PD PWB Y (LSU): 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Laser scanner unit and LSU relay PWB (YC12) LSU relay PWB (YC3) and Engine PWB (YC12) 2. If the FCC wiring is disconnected, replace the FCC wiring. 3. Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 4300
  • Description: Polygon motor phase error
    ASIC won’t settle in completion of phase adjustment for 2 s after a BD signal is detected.
  • Remedy: Laser scanner unit: Replace the laser scanner unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 4600
  • Description: LSU cleaning motor error
    After LSU cleaning motor is driven, the ready signal does not turn to L within 2 s. After LSU cleaning motor is stabilized, the ready signal is at the H level for 1 s continuously.
  • Remedy: LSU cleaning motoror: 1. Execute LSU cleaning using Adjustment/Maintenance of the system menu. 2. Rotate the drive gear and the cleaning spiral by the hand and check that they are not unusually loaded, and replace if it is damaged. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. LSU cleaning motor and Engine PWB (YC21) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the LSU cleaning motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 5101
  • Description: Main high-voltage error K
    Measure the inflowing current when Vpp is varied in 3 steps and verify if the difference of the currents of 0 and step 2 is less than 42 (51 if lower highvoltage board).
  • Remedy: Drum unit: 1. Execute U030 Belt Mean Drum Motor and check that the drum motor can rotate. 2. Confirm that the drum or the drum screw can rotate. 3. Check that the discharger lamp is properly connected. 4. If it won’t rotate, replace the drum unit.
    Charger roller unit: 1. Check that the high-voltage contacts are not distorted or adhered with foreign objects. 2. Reinstall the chrager roller unit.Or, replace the charger roller unit.
    High voltage PWB 1: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. High voltage PWB 1(YC4)*1,(YC3)*2 and Engine PWB (YC17) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the High voltage PWB 1. *1:45 ppm model/ 55ppm model *2:30ppm model/ 35ppm model
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 5102
  • Description: Main high-voltage error C
    Measure the inflowing current when Vpp is varied in 3 steps and verify if the difference of the currents of 0 and step 2 is less than 42 (51 if lower highvoltage board).
  • Remedy: Drum unit: 1. Execute U030 Belt Mean Drum Motor and check that the drum motor can rotate. 2. Confirm that the drum or the drum screw can rotate. 3. Check that the discharger lamp is properly connected. 4. If it won’t rotate, replace the drum unit.
    Charger roller unit: 1. Check that the high-voltage contacts are not distorted or adhered with foreign objects. 2. Reinstall the chrager roller unit.Or, replace the charger roller unit.
    High voltage PWB 1: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. High voltage PWB 1(YC2) and Engine PWB (YC16) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the High voltage PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 5103
  • Description: Main high-voltage error M
    Measure the inflowing current when Vpp is varied in 3 steps and verify if the difference of the currents of 0 and step 2 is less than 42 (51 if lower highvoltage board).
  • Remedy: Drum unit: 1. Execute U030 Belt Mean Drum Motor and check that the drum motor can rotate. 2. Confirm that the drum or the drum screw can rotate. 3. Check that the discharger lamp is properly connected. 4. If it won’t rotate, replace the drum unit.
    Charger roller unit: 1. Check that the high-voltage contacts are not distorted or adhered with foreign objects. 2. Reinstall the chrager roller unit.Or, replace the charger roller unit.
    High voltage PWB 1: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. High voltage PWB 1(YC3) and Engine PWB (YC17) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the High voltage PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 5104
  • Description: Main high-voltage error Y
    Measure the inflowing current when Vpp is varied in 3 steps and verify if the difference of the currents of 0 and step 2 is less than 42 (51 if lower highvoltage board).
  • Remedy: Drum unit: 1. Execute U030 Belt Mean Drum Motor and check that the drum motor can rotate. 2. Confirm that the drum or the drum screw can rotate. 3. Check that the discharger lamp is properly connected. 4. If it won’t rotate, replace the drum unit.
    Charger roller unit: 1. Check that the high-voltage contacts are not distorted or adhered with foreign objects. 2. Reinstall the chrager roller unit.Or, replace the charger roller unit.
    High voltage PWB 1: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. High voltage PWB 1(YC1) and Engine PWB (YC16) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the High voltage PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6000
  • Description: Broken fuser heater wire
    Fuser thermistor 1 does not reach 100° C/212 °F even after 60 s during warming up. The detected temperature of fuser thermistor 1 does not reach the specified temperature (ready indication temperature) for 420 s in warming up after reached to 100° C/212 °F.
  • Remedy: Fuser unit: 1. Check that no paper jam is present. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Fuser unit and execute U167 counter clear. (Deteriorated sensitivity due to the toner adhered to the center thermistor.)
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6020
  • Description: Abnormally high fuser Center thermistor 1 temperature
    Fuser center thermistor 1 detects a temperature higher than 240°C/464°F for 1 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6030
  • Description: Broken fuser center thermistor 1 wire
    Input from fuser center thermistor 1 is 1010 or more (A/D value) continuously for 1 s. Verify if A/D read in the differential output won’t change by 4 or more when it was turned on for 10 seconds.
  • Remedy: Fuser unit: 1. Check that no paper jam is present. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Fuser unit and execute U167 counter clear. (Deteriorated sensitivity due to the toner adhered to the center thermistor.)
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. Replace the Fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6040
  • Description: Fuser heater error
    Input from fuser thermistor 1 is abnormal value continuously for 1 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB (YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
  • Code: 6050
  • Description: Abnormally low fuser center thermistor 1 temperature
    Fuser center thermistor 1 detects a temperature lower than 100°C/212°F for 1 s after warming up, during ready or during print. The temperature of thermistor 1 is detected to be less than 70°C/158°F for more than one second during lowpower mode.
  • Remedy: Power source: 1. Check that the operating voltage falls within +/-10%. 2. Check no voltage drop is caused. The heater is deactivated at 70V or lower. 3. Relocate the AC outlet that supplies power.
    Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. Replace the Fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6120
  • Description: Abnormally high fuser press thermistor 4 temperature
    Fuser press thermistor 4 detects a temperature higher than 190°C/374°F for 1 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6130
  • Description: Broken fuser press thermistor 4 wire
    Input from fuser press thermistor 4 is 992 or more (A/D value) continuously for 60 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) Fuser IH PWB(YC4) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6150
  • Description: Abnormally low fuser press thermistor 4 temperature Fuser press thermistor 4 detects a temperature lower than 30°C/86°F for 1 s after warming up.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) If the wiring is disconnected, shorted or grounded, replace the wiring. 2. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6200
  • Description: Broken fuser edge heater wire
    Fuser edge thermistor 2 does not reach 100° C/212 °F even after 60 s during warming up. The detected temperature of fuser edge thermistor 2 does not reach the specified temperature (ready indication temperature) for 420 s in warming up after reached to 100° C/212 °F.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6220
  • Description: Abnormally high fuser edge thermistor 2 temperature
    Fuser edge thermistor 2 detects a temperature higher than 245°C/473°F for 1 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6230
  • Description: Broken fuser edge thermistor 2 wire
    The Input signal from the fuser edge thermistor 2 is 992 or more (A/D value) continuously for 1 s when the temperature at the fuser edge thermistor 1 is higher than 100°C/212°F during warming up.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
  • Code: 6250
  • Description: Abnormally low fuser edge thermistor 2 temperature
    Fuser edge thermistor 2 detects a temperature lower than 100°C/212°F for 1 s during ready or print. Fuser edge thermistor 2 detects a temperature lower than 50°C/122°F for 1 s during low power mode.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
    Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
  • Code: 6320
  • Description: Abnormally high fuser middle thermistor 3 temperature
    Fuser middle thermistor 3 detects a temperature higher than 205°C/401°F for 1 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6330
  • Description: Broken fuser center thermistor 3 wire
    Fuser center thermistor 3 detects a temperature lower than 20°C/68°F continuously for 1 s.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
  • Code: 6600
  • Description: Fuser belt rotation error
    A belt rotating pulse is not received for 1 s. (Engine CPU)
  • Remedy: Fuser motor: 1. To check the motor operation, execute U030 Fuser. 2. Check that the drive gear can rotate and not heavily loaded and, if necessary, apply grease to the axle holder and gears. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser motor and Feed PWB (YC18) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the fuser motor.
    Fuser belt sensor: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6610
  • Description: Fuser release sensor error
    The fusing pressure release sensor won’t send an off signal in 5 seconds since a pressure release instruction is given for the fusing pressure motor. The fusing pressure release sensor won’t send an on signal in 5 seconds since a pressure instruction is given for the fusing pressure motor.
  • Remedy: Fuser release motor: 1. To check the motor operation, execute U030 Fuser Release. 2. Check that the drive gear can be rotated and the separation is possible. 3. If the motor won’t rotate, confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the fuser unit and execute U167 counter clear.
    Fuser release sensor: 1. Check that the sensor is correctly positioned. 2. Check that the sensor is not contaminated or damaged.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6710
  • Description: Fuser IH PWB CPU reset error
    Watch doc timer has been overflowed.
  • Remedy: Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6720
  • Description: Fuser IH belt rotation error
    While driving, the pulse count is less than 3 for 2 seconds during the input to the rotation pulse signal is 200 msec.
  • Remedy: Fuser motor: 1. To check the motor operation, execute U030 Fuser. 2. Check that the drive gear can rotate and not heavily loaded and, if necessary, apply grease to the axle holder and gears. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser motor and Feed PWB (YC18) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the fuser motor.
    Fuser belt sensor: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser unit and execute U167 counter clear.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. Replace the fuser IH PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6730
  • Description: Abnormally high fuser IH PWB temperature 1 (IGBT1)
    The input detect temperature is higher than 115°C/221 °F.
  • Remedy: Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6740
  • Description: Abnormally high fuser IH PWB temperature 2 (IGBT2)
    The input detect temperature is higher than 115°C/221 °F.
  • Remedy: Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6750
  • Description: Fuser IH output over-current error
    The output current of IH CPU is higher than 90A for 10 ms in succession.
  • Remedy: Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6760
  • Description: Fuser IH input over-current error
    The input current of IH CPU is higher than 20A(100V/120V), 10A(200V) for 100 ms in succession.
  • Remedy: Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6770
  • Description: Fuser IH low electric power error
    Less than 0.6 times of the preset power is detected for 120 ms in succession after the IH heater remote has turned on.
  • Remedy: Fuser unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser unit and Fuser IH PWB (YC6) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser IH unit.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser IH PWB.
    Fuser IH unit: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH unit and Fuser IH PWB (YC9 and 10) Fuser IH PWB( YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the fuser IH unit.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6900
  • Description: Fuser belt cooling fan error
    When the fuser edge fan motor 1 , 2 is driven, alarm signal is detected for 5 s continuously.
  • Remedy: Fuser edge fan motor 1, 2: 1. To check the fan motor operation, execute U037 Fuser Edge. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser edge fan motor 1 and Engine PWB (YC26) Fuser edge fan motor 2 and Fuser PWB (YC2) Fuser PWB (YC1) and Engine PWB (YC26) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the fuser unit and execute U167 counter clear.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6910
  • Description: Engine software ready error
    The device won’t engage in ready state in 60 minutes after warming-up has began. (A previous timeout process has not been cancelled.)
  • Remedy: Engine PWB: 1. Turn the main power switch off and after 5 seconds, turn it on. 2. Reinstall the engine software. 3. Replace the engine PWB.
  • Code: 6920
  • Description: Fuser front fan motor error
    When the fuser front fan motor is driven, alarm signal is detected for 5 s continuously.
  • Remedy: Fuser front fan motor: 1. To check the fan motor operation, execute U037 IH Coil. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser front fan motor and Front PWB (YC4) Front PWB (YC3) and Engine PWB (YC7) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the fuser front fan motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6930
  • Description: Fuser rear fan motor error
    When the fuser rear fan motor is driven, alarm signal is detected for 5 s continuously.
  • Remedy: Fuser rear fan motor: 1. To check the fan motor operation, execute U037 Fuser Coling. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser rear fan motor and Engine PWB (YC26) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the fuser rear fan motor.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6940
  • Description: IH PWB cooling fan motor error
    When the IH fan motor is driven, the alarm signal is detected for 5 s continuously.
  • Remedy: IH fan motor: 1. To check the fan motor operation, execute U037 IH Pwb. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. IH fan motor and Feed PWB 1(YC11) Feed PWB 1(YC2) and Engine PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the IH fan motor.
    Feed PWB 1: Replace the Feed PWB1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 6950
  • Description: Fuser IH PWB communication error
    No response is received in 30 ms since a command is sent to IHCPU. A checksum error is detected 10 times in succession.
  • Remedy: Power source PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Power source PWB (YC9) and Feed PWB 1(YC4) Power source PWB (YC3) and Fuser IH PWB (YC1) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. If the +24V output is not given by the power source PWB (YC9), replace the power source PWB.
    Feed PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Power source PWB (YC3) and Fuser IH PWB (YC1) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. If the +24V output is not given by the feed PWB1 (YC27), replace the feed PWB1.
    Fuser IH PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Fuser IH PWB(YC4) and Engine PWB (YC26) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Fuser IH PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 6960
  • Description: Current PWB error
    The power current is greater than 1A for 5 seconds continuously despite that 500W was indicated as the fuser power during power-up. (45 ppm/ 55 ppm model only)
  • Remedy: Current PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Current PWB(YC17) and Feed PWB2 (YC13) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Current PWB.
  • Code: 6990
  • Description: Fuser power supply incompatibility
    Information won’t match between the engine backup and the fuser IH PWB.
  • Remedy: Differences in settings after initialization: When this has happened after initialization using U021, make settings identical with the voltages on the IH PWB using U169.
    Fuser IH PWB: Replace with a fuser IH PWB specifically designed with the standard voltage.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7001
  • Description: Toner motor K error
    A state that the pulse is not detected at the pulse sensor for 200 ms has occurred more than 15 times in a row during the toner motor K is driven. A state that the TMOT_LOCK signal becomes H (locked) is detected after 200 ms when the toner motor K is driven has occurred 15 sets in total.
  • Remedy: Toner container K: 1. Check that the spiral screw of the toner container can be rotated by the hand. 2. Check for broken gears and replace if any.
    Toner motor K: 1. Draw out the toner container and execute U135 to check the toner motor operation . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor K and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor K.
    Screw sensor K: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Screw sensor K and Engine PWB (YC27) 3. Replace the screw sensor K.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7002
  • Description: Toner motor C error
    A state that the pulse is not detected at the pulse sensor for 200 ms has occurred more than 15 times in a row during the toner motor C is driven. A state that the TMOT_LOCK signal becomes H (locked) is detected after 200 ms when the toner motor C is driven has occurred 15 sets in total.
  • Remedy: Toner container C: 1. Check that the spiral screw of the toner container can be rotated by the hand. 2. Check for broken gears and replace if any.
    Toner motor C: 1. Draw out the toner container and execute U135 to check the toner motor operation . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor C and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor C.
    Screw sensor C: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Screw sensor C and Engine PWB (YC27) 3. Replace the screw sensor C.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 7003
  • Description: Toner motor M error
    A state that the pulse is not detected at the pulse sensor for 200 ms has occurred more than 15 times in a row during the toner motor M is driven. A state that the TMOT_LOCK signal becomes H (locked) is detected after 200 ms when the toner motor M is driven has occurred 15 sets in total.
  • Remedy: Toner container M: 1. Check that the spiral screw of the toner container can be rotated by the hand. 2. Check for broken gears and replace if any.
    Toner motor M: 1. Draw out the toner container and execute U135 to check the toner motor operation . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor M and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor M.
    Screw sensor M: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Screw sensorM and Engine PWB (YC27) 3. Replace the screw sensor M.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7004
  • Description: Toner motor Y error
    A state that the pulse is not detected at the pulse sensor for 200 ms has occurred more than 15 times in a row during the toner motor Y is driven. A state that the TMOT_LOCK signal becomes H (locked) is detected after 200 ms when the toner motor Y is driven has occurred 15 sets in total.
  • Remedy: Toner container Y: 1. Check that the spiral screw of the toner container can be rotated by the hand. 1. Check for broken gears and replace if any.
    Toner motor Y: 1. Draw out the toner container and execute U135 to check the toner motor operation . 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor Y and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor Y.
    Screw sensor Y: 1. Check that the sensor is correctly positioned. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Screw sensor Y and Engine PWB (YC27) 3. Replace the screw sensor Y.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7101
  • Description: Toner sensor K error
    Sensor output value of 60 or less or 944 or more continued for 3 s.
  • Remedy: Failure of locking the developer waste slot at setup:
    If an abnormal noise is heard, check that the developer ejection outlet is released and, if not, release the outlet.
    Toner sensor K: 1. Check the toner sensor output by U155. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner sensor K and Front PWB (YC9) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Check that the gears of the developer unit K are not damaged and the spiral can rotate. 5. Replace the Developer unit K.
    Toner motor K: 1. Draw out the toner container and execute U135 to check the toner motor operation. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor K and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor K.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7102
  • Description: Toner sensor C error Sensor output value of 60 or less or 944 or more continued for 3 s.
  • Remedy: Failure of locking the developer waste slot at setup:
    If an abnormal noise is heard, check that the developer ejection outlet is released and, if not, release the outlet.
    Toner sensor C: 1. Check the toner sensor output by U155. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner sensor C and Front PWB (YC13) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Check that the gears of the developer unit C are not damaged and the spiral can rotate. 5. Replace the Developer unit C.
    Toner motor C: 1. Draw out the toner container and execute U135 to check the toner motor operation. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor C and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor C.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7103
  • Description: Toner sensor M error
    Sensor output value of 60 or less or 944 or more continued for 3 s.
  • Remedy: Failure of locking the developer waste slot at setup:
    If an abnormal noise is heard, check that the developer ejection outlet is released and, if not, release the outlet.
    Toner sensor M: 1. Check the toner sensor output by U155. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner sensor M and Front PWB (YC11) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Check that the gears of the developer unit M are not damaged and the spiral can rotate. 5. Replace the Developer unit M.
    Toner motor M: 1. Draw out the toner container and execute U135 to check the toner motor operation. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor M and ?Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor M.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7104
  • Description: Toner sensor Y error
    Sensor output value of 60 or less or 944 or more continued for 3 s.
  • Remedy: Failure of locking the developer waste slot at setup:
    If an abnormal noise is heard, check that the developer ejection outlet is released and, if not, release the outlet.
    Toner sensor Y: 1. Check the toner sensor output by U155. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner sensor Y and Front PWB (YC15) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Check that the gears of the developer unit Y are not damaged and the spiral can rotate. 5. Replace the Developer unit Y.
    Toner motor Y: 1. Draw out the toner container and execute U135 to check the toner motor operation. 2. Check the drive gear can rotate or they are not unusually loaded and, if necessary, replace. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Toner motor Y and Engine PWB (YC27) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the Toner motor Y.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7200
  • Description: Broken outer temperature sensor 2 wire
    The sensor input sampling is greater than 230.
  • Remedy: Outer temperature sensor 2:
    1. Confirm Ext/Int is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Outer temperature sensor 2 and Front PWB (YC19) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the outer temperature sensor 2.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7210
  • Description: Short-circuited outer temperature sensor 2
    The sensor input sampling is less than 69.
  • Remedy: Outer temperature sensor 2:
    1. Confirm Ext/Int is displayed by U139 temperature and humidity . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Outer temperature sensor 2 and Front PWB (YC19) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the outer temperature sensor 2.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7221
  • Description: Broken LSU thermistor K wire
    The sensor input sampling is greater than 230.
  • Remedy: LSU thermistor K: 1. Confirm LSU is displayed by U139 temperature and humidity . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC5) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7222
  • Description: Broken LSU thermistor C wire
    The sensor input sampling is greater than 230.
  • Remedy: LSU thermistor C: 1. Confirm LSU is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC10) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7223
  • Description: Broken LSU thermistor M wire
    The sensor input sampling is greater than 230.
  • Remedy: LSU thermistor M: 1. Confirm LSU is displayed by U139 temperature and humidity . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC8) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7224
  • Description: Broken LSU thermistor Y wire
    The sensor input sampling is greater than 230.
  • Remedy: LSU thermistor Y: 1. Confirm LSU is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC12) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7231
  • Description: Short-circuited LSU thermistor K
    The sensor input sampling is less than 69.
  • Remedy: LSU thermistor K: 1. Confirm LSU is displayed by U139 temperature and humidity . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC5) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: Replace the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7232
  • Description: Short-circuited LSU thermistor C
    The sensor input sampling is less than 69.
  • Remedy: LSU thermistor C: 1. Confirm LSU is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC10) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7233
  • Description: Short-circuited LSU thermistor M
    The sensor input sampling is less than 69.
  • Remedy: LSU thermistor M: 1. Confirm LSU is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC8) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7234
  • Description: Short-circuited LSU thermistor Y
    The sensor input sampling is less than 69.
  • Remedy: LSU thermistor Y: 1. Confirm LSU is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Laser scanner unit and LSU relay PWB (YC12) LSU relay PWB (YC3) and Engine PWB (YC12) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the laser scanner unit.
    LSU relay PWB: REPLACE the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7241
  • Description: Broken developer thermistor K wire
    The sensor input sampling is greater than 230.
  • Remedy: Developer thermistor K: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit K and Front PWB (YC9) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit K.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7242
  • Description: Broken developer thermistor C wire
    The sensor input sampling is greater than 230.
  • Remedy: Developer thermistor C: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit C and Front PWB (YC13) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit C.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7243
  • Description: Broken developer thermistor M wire
    The sensor input sampling is greater than 230.
  • Remedy: Developer thermistor M: 1. Confirm Developing is displayed by U139 temperature and humidity . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit M and Front PWB (YC11) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit M.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7244
  • Description: Broken developer thermistor Y wire
    The sensor input sampling is greater than 230.
  • Remedy: Developer thermistor Y: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit Y and Front PWB (YC15) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit Y.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7251
  • Description: Short-circuited developer thermistor K
    The sensor input sampling is less than 69.
  • Remedy: Developer thermistor K: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit K and Front PWB (YC9) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit K.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7252
  • Description: Short-circuited developer thermistor C
    The sensor input sampling is less than 69.
  • Remedy: Developer thermistor C: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit C and Front PWB (YC13) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit C.
    Front PWB: Replace the front
    PWB.Engine: PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7253
  • Description: Short-circuited developer thermistor M:The sensor input sampling is less than 69.
  • Remedy: Developer thermistor M: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit M and Front PWB (YC11) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit M:
  • Code: 7254
  • Description: Short-circuited developer thermistor Y wire
    The sensor input sampling is less than 69.
  • Remedy: Developer thermistor Y: 1. Confirm Developing is displayed by U139 temperature and humidity. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit Y and Front PWB (YC15) Front PWB (YC2) and Engine PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the Developer unit Y.
    Front PWB: Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7401
  • Description: Developer unit K type mismatch error
    Improper adaptation of the machine and developer unit K is detected.
  • Remedy: Different type of the developer unit is installed: Install the developer unit of the correct type.
    Developer unit K: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit K and Front PWB (YC9) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring.
  • Code: 7402
  • Description: Developer unit C type mismatch error
    Improper adaptation of the machine and developer unit C is detected.
  • Remedy: Different type of the developer unit is installed: Install the developer unit of the correct type.
    Developer unit C: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit C and Front PWB (YC13) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring.
  • Code: 7403
  • Description: Developer unit M type mismatch error
    Improper adaptation of the machine and developer unit M is detected.
  • Remedy: Different type of the developer unit is installed: Install the developer unit of the correct type.
    Developer unit M: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit M and Front PWB (YC11) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring.
  • Code: 7404
  • Description: Developer unit Y type mismatch error
    Improper adaptation of the machine and developer unit Y is detected.
  • Remedy: Different type of the developer unit is installed: Install the developer unit of the correct type.
    Developer unit Y: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit Y and Front PWB (YC15) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring.
  • Code: 7601
  • Description: ID sensor 1 error
    An abnormal value is detected in the input data to ID sensor 1. Dark potential error FrontDarkP and FrontDarkS are greater than 0.80V. Light potential error FrontBrightS is smaller than FrontDarkS. FrontBrightP is smaller than [FrontDarkP + 0.5V].
  • Remedy: ID sensor1 (front): 1. Execute U464 Calib for setting ID compensation operation and check the displayed values by U465 Boas Calib for ID compensation reference. 2. Detach the imtermediate intermediate transfer belt unit and clean the ID sensor on its surface. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. ID sensor 1 (front) and Feed PWB 1(YC10) Feed PWB 1(YC1) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring.
    Feed PWB: 1 Replace the Feed PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7602
  • Description: ID sensor 2 error
    Dark potential error RearDarkP and RearDarkS are greater than 0.80V. Light potential error RearBrightS is smaller than RearDarkS. RearBrightP is smaller than [RearDarkP + 0.5V].
  • Remedy: ID sensor 2 (rear): 1. Execute U464 Calib for setting ID compensation operation and check the displayed values by U465 Boas Calib for ID compensation reference. 2. Detach the imtermediate intermediate transfer belt unit and clean the ID sensor on its surface. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. ID sensor2 (rear) and Feed PWB 1(YC10) Feed PWB 1(YC1) and Engine PWB (YC6) 4. If the wiring is disconnected, shorted or grounded, replace the wiring.
    Feed PWB: 1 Replace the Feed PWB 1.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7800
  • Description: Broken outer temperature sensor 1 wire
    The device did not respond for more than 5 ms during reading, in 5 times.
  • Remedy: Outer temperature sensor 1: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Outer temperature sensor 1 and Front PWB (YC16) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Outer temperature sensor 1.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 7901
  • Description: Drum K EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: DR PWB-K: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DR PWB-K and Front PWB (YC7) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum unit K.
    Front PWB: Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7902
  • Description: Drum C EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: DR PWB- C: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DR PWB- C and Front PWB (YC12) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum unit C.
    Front PWB: Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB5 times.
  • Code: 7903
  • Description: Drum M EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: DR PWB- M: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DR PWB- M and Front PWB (YC10) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum unit M.
    Front PWB: Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7904
  • Description: Drum Y EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: DRPWB- Y: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DRPWB- Y and Front PWB (YC14) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Drum unit Y.
    Front PWB Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 7911
  • Description: Developer unit K EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: Developer unit K: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit K and Front PWB (YC9) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Developer unit K.
    Front PWB: Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7912
  • Description: Developer unit C EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: Developer unit C: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit C and Front PWB (YC13) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Developer unit C.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB5 times.
  • Code: 7913
  • Description: Developer unit M EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: Developer unit M: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit M and Front PWB (YC11) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Developer unit M.
    Front PWB: Replace the front PWB.
    Engine PWB 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7914
  • Description: Developer unit Y EEPROM error
    No response is issued from the device in reading/writing for 5 ms or more and this problem is repeated five times successively. Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: Developer unit Y: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Developer unit Y and Front PWB (YC15) Front PWB (YC2) and Engine PWB (YC10) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Developer unit Y.
    Front PWB: Replace the front PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB5 times.
  • Code: 7941
  • Description: Laser scanner unit K EEPROM error
    [35 ppm/ 45 ppm/ 55 ppm model] Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: APC PWB K: 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. APC PWB K and LSU relay PWB (YC5) LSU relay PWB (YC2) and Engine PWB (YC11) 2. If the FCC wiring is disconnected, shorted or grounded, replace the FCC wiring. 3. Replace the laser scanner unit.
    LSU relay PWB: Replace the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB.
  • Code: 7942
  • Description: Laser scanner unit C EEPROM error
    [35 ppm/ 45 ppm/ 55 ppm model] Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: APC PWB C: 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. APC PWB C and LSU relay PWB (YC10) LSU relay PWB (YC2) and Engine PWB (YC11) 2. If the FCC wiring is disconnected, shorted or grounded, replace the FCC wiring. 3. Replace the laser scanner unit.
    LSU relay PWB: Replace the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB5 times.
  • Code: 7943
  • Description: Laser scanner unit M EEPROM error
    [35 ppm/ 45 ppm/ 55 ppm model] Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: APC PWB M: 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. APC PWB M and LSU relay PWB (YC8) LSU relay PWB (YC2) and Engine PWB (YC11) 2. If the FCC wiring is disconnected, shorted or grounded, replace the FCC wiring. 3. Replace 1-5-43the laser scanner unit.
    LSU relay PWB: Replace the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB5 times.
  • Code: 7944
  • Description: Laser scanner unit Y EEPROM error
    [35 ppm/ 45 ppm/ 55 ppm model] Mismatch of reading data from two locations occurs 8 times successively. Mismatch between writing data and reading data occurs 8 times successively.
  • Remedy: APC PWB Y 1. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. APC PWB Y and LSU relay PWB (YC12) LSU relay PWB (YC2) and Engine PWB (YC11) 2. If the FCC wiring is disconnected, shorted or grounded, replace the FCC wiring. 3. Replace the laser scanner unit.
    LSU relay PWB: Replace the LSU relay PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 8010
  • Description: Punch motor 1 error
    When the punch motor is driven, punch home position sensor does not turn on within 200 ms
  • Remedy: Punch motor 1. Execute U240 Motor — Punch to check the finisher operation. 2. Manipulate the punch up and down to check it can smoothly move up and down. 3. Check that the drive from the motor reaches the punch cam. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch motor and Punch PWB (YC4) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the punch motor.
    Punch home position sensor: 1. Execute U241 Punch — Punch HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch home position sensor and Punch PWB (YC8) 4. Replace the Punch home position sensor.
    Punch PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch PWB (YC1) and DF main PWB (YC7) (4000-sheet finisher) Punch PWB (YC1) and DF main PWB (YC8) (1000-sheet finisher) 2. Replace the punch PWB.
    DF main PWB: Replace the DF main PWB.
  • Code: 8020
  • Description: Punch motor 2 error
    Home position is not obtained in 3 s after home position is initialized or in standby.
  • Remedy: Punch motor: 1. Execute U240 Motor — Punch to check the finisher operation . 2. Manipulate the punch up and down to check it can smoothly move up and down. 3. Check that the drive from the motor reaches the punch cam. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch motor and Punch PWB (YC4) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the punch motor.
    Punch PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch PWB (YC1) and DF main PWB (YC7)(4000-sheet finisher) Punch PWB (YC1) and DF main PWB (YC8)(1000-sheet finisher) 2. Replace the punch PWB.
    DF main PWB: Replace the DF main PWB
  • Code: 8030
  • Description: Punch motor 3 error
    Home position does not turn from On to Off in 50 ms after home position has been initialized.{?
  • Remedy: Punch motor: 1. Execute U240 Motor — Punch to check the finisher operation. 2. Manipulate the punch up and down to check it can smoothly move up and down. 3. Check that the drive from the motor reaches the punch cam. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch motor and Punch PWB (YC4) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the punch motor.
    Punch PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch PWB (YC1) and DF main PWB (YC7) (4000-sheet finisher) Punch PWB (YC1) and DF main PWB (YC8) (1000-sheet finisher) 2. Replace the punch PWB.
    DF main PWB: Replace the DF main PWB
  • Code: 8090
  • Description: DF paddle motor error
    When the DF paddle motor is driven, DF paddle sensor does not turn on within 1 s.
  • Remedy: DF paddle motor: 1. Execute U240 Motor — Beat to check the finisher operation. 2. Check that the paddle can rotate. 3. Check that the drive from the motor reaches the paddle. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF paddle motor and DF main PWB (YC15) (4000-sheet finisher) DF paddle motor and DF main PWB (YC11) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF paddle motor.
    DF paddle sensor: 1. Execute U241 Finisher — Bundle Eject HP to check the finisher switch. 2. Check that the sensor and its mounting board are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF paddle sensor and DF main PWB (YC22) (4000-sheet finisher) DF paddle sensor and DF main PWB (YC20) (1000-sheet finisher) 4. Replace the DF paddle sensor.
    DF main PWB: Replace the DF main PWB.
  • Code: 8100
  • Description: DF eject release motor error
    When the DF eject release motor is driven, DF bundle discharge sensor does not turn on within 1 s.
  • Remedy: DF eject release motor DF bundle discharge unit sensor: 1. Execute Motor — Eject Unlock (Full) of U240 finisher operation check. 2. Check that the eject guide of the process tray is opened and, if not, correct the guide. 3. Check that the drive from the motor reaches the eject guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF bundle discharge unit sensor and DF main PWB (YC22)(4000-sheet finisher) DF bundle discharge unit sensor and DF main PWB (YC20)(1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF eject release motor.
    DF bundle discharge unit sensor: 1. Execute Finisher — Bundle Eject HP of U241 finisher switch check. 2. Check that the sensor and its mounting board are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF bundle discharge unit sensor and DF main PWB (YC22)(4000-sheet finisher) DF bundle discharge unit sensor and DF main PWB (YC20)(1000-sheet finisher) 4. Replace the DF bundle discharge unit sensor.
    DF main PWB: Replace the DF main PWB.
  • Code: 8110
  • Description: DF shift motor 1 error
    (4000-sheet finisher) DF shift sensor 1 won’t turn on when it has travelled 160 mm after DF shift motor 1 is driven.
  • Remedy: DF shift motor 1 [front]: 1. Execute U240 Motor — Sort Test to check the finisher operation. 2. Manipulate the front shift guide back and forth to check that it is smoothly operable. 3. Check that the drive from the motor reaches the front shift guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF shift motor 1 and DF main PWB (YC14) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF shift motor 1
    DF shift sensor 1 [front]: 1. Execute U241 Finisher — Shift Front HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF shift sensor 1 and DF main PWB (YC23) 4. Replace the DF shift sensor 1.
    DF main PWB: Replace the DF main PWB.
  • Code: 8120
  • Description: DF shift motor 2 error
    (4000-sheet finisher) DF shift sensor 1 won’t turn on when it has travelled 160 mm after DF shift motor 1 is driven.
  • Remedy: DF shift motor 2 [rear]: 1. Execute U240 Motor — Sort Test to check the finisher operation. 2. Manipulate the rear shift guide back and forth to check it is smoothly operable. 3. Check that the drive from the motor reaches the rear shift guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF shift motor 2 and DF main PWB (YC14) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF shift motor 2.
    DF shift set sensor 2 [rear]: 1. Execute U241 Finisher — Shift Trail HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF shift sensor 2 and DF main PWB (YC23) 4. Replace the DF shift set sensor2.
    DF main PWB: Replace the DF main PWB
  • Code: 8130
  • Description: DF shift release motor error
    (4000-sheet finisher) When the DF shift release motor is driven, DF shift release sensor does not turn on within 1 s.
  • Remedy: DF shift release motor: 1. Check that cancelling the maintenance mode after executing U240 Motor — Sort for the finisher operation check lets the rear and forth cursors return to the home position. 2. Manipulate the shift guide back and forth to check it is smoothly operable. 3. Check that the drive from the motor reaches the shift guide front and rear. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF shift release motor and DF main PWB (YC23) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF shift release motor.
    DF shift release sensor: 1. Execute U241 Finisher — Shift Unlock HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF shift release sensor and DF main PWB (YC23) 4. Replace the DF shift release sensor.
    DF main PWB: Replace the DF main PWB.
  • Code: 8140
  • Description: DF tray motor error 1
    When the main tray has ascended, DF tray sensor 1 or DF tray upper surface sensor does not turn on within 20 s.
  • Remedy: DF tray motor: 1. Execute U240 Motor — Tray to check the finisher operation. 2. Manipulate the main tray up and down to check it is smoothly operable. 3. Check that the drive from the motor reaches the main tray. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF tray motor and DF Main PWB(YC16) (4000-sheet finisher) DF tray motor and DF Main PWB(YC14) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF tray motor.
    DF tray sensor 1 DF tray upper surface sensor: 1. Execute U241 Finisher — Tray U-Limit, Tray Top to check the finisher switch . 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF tray sensor 1 and DF Main PWB(YC22) (4000-sheet finisher) DF tray upper surface sensor and DF Main PWB(YC21,YC13) (4000-sheet finisher) DF tray sensor 1 and DF main PWB (YC20) (1000-sheet finisher) DF tray upper surface sensor and DF main PWB (YC18) (1000-sheet finisher) 4. Replace the DF tray sensor 1 or DF tray upper surface sensor.
    DF main PWB: Replace the DF main PWB.
  • Code: 8150
  • Description: DF tray motor error 2
    When the main tray has descended, DF tray sensor 1 or DF tray upper surface sensor does not turn off within 5 s.
  • Remedy: DF tray motor: 1. Execute U240 Motor — Tray to check the finisher operation. 2. Manipulate the main tray up and down to check it is smoothly operable. 3. Check that the drive from the motor reaches the main tray. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF tray motor and DF main PWB (YC16) (4000-sheet finisher) DF tray motor and DF main PWB (YC14) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF tray motor.
    DF tray sensor 1 DF tray upper surface sensor: 1. Execute U241 Finisher — Tray U-Limit, Tray Top to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF tray sensor 1 and DF main PWB (YC22) (4000-sheet finisher) DF tray upper surface sensor and DF main PWB (YC21,YC13) (4000-sheet finisher) DF tray sensor 1 and DF main PWB (YC20) (1000-sheet finisher) DF tray upper surface sensor and DF main PWB (YC18) (1000-sheet finisher) 4. Replace the DF tray sensor 1 or DF tray upper surface sensor.
    DF main PWB: Replace the DF main PWB.
  • Code: 8160
  • Description: DF tray motor error 3
    When the main tray has descended, DF tray sensor 3 does not turn on within 20 s.
  • Remedy: DF tray motor: 1. Execute U240 Motor — Tray to check the finisher operation. 2. Manipulate the main tray up and down to check it is smoothly operable. 3. Check that the drive from the motor reaches the main tray. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF tray motor and DF main PWB (YC16) (4000-sheet finisher) DF tray motor and DF main PWB (YC14) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF tray motor.
    DF tray sensor 4: 1. Execute U241 Finisher — Tray Middle to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF tray sensor 4 and DF main PWB (YC23) (4000-sheet finisher) DF tray sensor 4 and DF main PWB (YC20) (1000-sheet finisher) 4. Replace the DF tray sensor 4.
    DF main PWB: Replace the DF main PWB
  • Code: 8170
  • Description: DF side registration motor 1 error 1
    When initial operation, DF side registration sensor 1 does not turn on within 3 s.
  • Remedy: DF side registration motor 1: 1. Execute U240 Motor — Width Test to check the finisher operation. 2. Manipulate the front side registration guide to check it is smoothly operable. 3. Check that the drive from the motor reaches the front side registration guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration motor 1 and DF main PWB (YC15) (4000-sheet finisher) DF side registration motor 1 and DF main PWB (YC11) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF side registration motor 1.
    DF side registration sensor 1: 1. Execute U241 Finisher — Width Front to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration sensor 1. and DF main PWB (YC22) (4000-sheet finisher) DF side registration sensor 1. and DF main PWB (YC20) (1000-sheet finisher) 4. Replace the DF side registration sensor 1.
    DF main PWB: Replace the DF main PWB
  • Code: 8180
  • Description: DF side registration motor 1 error 2
    JAM6810 ( jam in front of width alignment) is detected twice.
  • Remedy: DF side registration motor 1: 1. Execute U240 Motor — Width Test to check the finisher operation. 2. Manipulate the front side registration guide back and forth to check it is smoothly operable. 3. Check that the drive from the motor reaches the front side registration guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration motor 1 and DF main PWB (YC15) (4000-sheet finisher) DF side registration motor 1 and DF main PWB (YC11) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF side registration motor 1.
    DF side registration sensor 1: 1. Execute U241 Finisher — Width Front to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration sensor 1. and DF main PWB (YC22) (4000-sheet finisher) DF side registration sensor 1. and DF main PWB (YC20) (1000-sheet finisher) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the DF side registration sensor 1.
    DF main PWB: Replace the DF main PWB.
  • Code: 8190
  • Description: DF side registration motor 2 error 1
    When initial operation, DF side registration sensor 2 does not turn on within 3 s.
  • Remedy: DF side registration motor 2: 1. Execute U240 Motor — Width Test to check the finisher operation. 2. Manipulate the rear side registration guide back and forth to check it is smoothly operable. 3. Check that the drive from the motor reaches the rear side registration guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration motor 2 and DF main PWB (YC15) (4000-sheet finisher) DF side registration motor 2 and DF main PWB (YC11) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF side registration motor 2.
    DF side registration sensor 2: 1. Execute U241 Finisher — Width tail HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration sensor 2 and DF main PWB (YC22) (4000-sheet finisher) DF side registration sensor 2 and DF main PWB (YC20) (1000-sheet finisher) 4. Replace the DF side registration sensor 2.
    DF main PWB: Replace the DF main PWB.
  • Code: 8200
  • Description: DF side registration motor 2 error 2
    JAM6910 ( jam in rear of width alignment) is detected twice.
  • Remedy: DF side registration motor 2: 1. Execute U240 Motor — Width Test to check the finisher operation. 2. Manipulate the rear side registration guide back and forth to check it is smoothly operable. 3. Check that the drive from the motor reaches the rear side registration guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration motor 2 and DF main PWB (YC15) (4000-sheet finisher) DF side registration motor 2 and DF main PWB (YC11) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF side registration motor 2.
    DF side registration sensor 2: 1. Execute U241 Finisher — Width tail HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF side registration sensor 2 and DF main PWB (YC22) (4000-sheet finisher) DF side registration sensor 2 and DF main PWB (YC20) (1000-sheet finisher) 4. Replace the DF side registration sensor 2.
    DF main PWB: Replace the DF main PWB.
  • Code: 8210
  • Description: DF slide motor error
    When initial operation, DF staple sensor does not turn on within 3 s.
  • Remedy: DF slide motor: 1. Execute U240 Motor — Staple Move to check the finisher operation. 2. Manipulate the staple unit back and forth to check it is smoothly operable. 3. Check that the drive from the motor reaches the staple unit. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF slide motor and DF main PWB (YC12) (4000-sheet finisher) DF slide motor and DF main PWB (YC10) (1000-sheet finisher) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DF slide motor.
    DF staple sensor: 1. Execute U241 Finisher — Width Staple HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF staple sensor and DF main PWB (YC22) (4000-sheet finisher) DF staple sensor and DF main PWB (YC20) (1000-sheet finisher) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the DF staple sensor.
    DF main PWB: Replace the DF main PWB.
  • Code: 8230
  • Description: DF staple motor error 1
    Staple JAM (DF) has been detected twice in a row. (The second JAM detection condition fullfilled with the home position did not detected in 600 ms after the motor was driven.)
  • Remedy: DF staple motor: 1. Remove the staple unit and check that stapling is possible without a jam. 2. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Staple unit and DF main PWB (YC17) (4000-sheet finisher) Staple unit and DF main PWB (YC11) (1000-sheet finisher) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the staple unit.
    DF staple sensor: Replace the staple unit.
    DF main PWB: Replace the DF main PWB
  • Code: 8240
  • Description: DF staple motor error 2
    Staple JAM (DF) has been detected twice in a row. (The second JAM detection condition fullfilled with a lock detection signal maintained 1 V for 500 ms continuously, while the stapler motor was driven.)
  • Remedy: DF staple motor: 1. Remove the staple unit and check that stapling is possible without a jam. 2. Confirm that the FCC wiring connector is not distorted and connect the FCC wiring all the way in. Staple unit and DF main PWB (YC17) (4000-sheet finisher) Staple unit and DF main PWB (YC11) (1000-sheet finisher) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the staple unit.
    DF main PWB: Replace the DF main PWB
  • Code: 8300
  • Description: Center-folding unit communication error
    (4000-sheet finisher) Communication with the center- folding unit is not possible.
  • Remedy: CF unit set switch: 1. Execute U241 Booklet — Set to check the finisher switch. 2. Check that the switch and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF main PWB (YC7) and DF main PWB (YC9) 4. If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the CF unit set switch.
    CF main PWB: Replace the CF main PWB.
    DF main PWB: Replace the DF main PWB.
  • Code: 8310
  • Description: CF side registration motor 2 error
    (4000-sheet finisher) When initial operation, CF side registration sensor 2 does not turn on within 1 s.
  • Remedy: CF side registration motor 2: 1. Execute Motor — Width Test of U240 finisher operation check . 2. Manipulate the side registration upper guide back and forth to check it can smoothly move back and forth. 3. Check that the drive from the motor reaches the side registration upper guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF side registration motor 2 and CF main PWB (YC10) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the CF side registration motor.
    CF side registration sensor 2: 1. Execute U241 Booklet — Width Up HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF side registration sensor 2 and CF main PWB (YC20) 4. Replace the CF side registration sensor 2.
    CF main PWB: Replace the CF main PWB
  • Code: 8320
  • Description: CF adjustment motor error
    (4000-sheet finisher) When initial operation, CF adjustment sensor does not turn on within 2.5 s.a
  • Remedy: CF adjustment motor1,2: 1. Execute U240 Motor — Bundle Up / Down to check the finisher operation . 2. Manipulate the fold moving belt up and down to check it is smoothly operable. 3. Check that the drive from the motor reaches the fold moving belt. (Check if the belt is bent.) 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF adjustment motor 1,2 and CF main PWB (YC10) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the CF adjustment motor1,2.
    CF adjustment sensor1,2: 1. Execute U241 Booklet — bundle Up / Down HP to check the finisher switch . 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF adjustment sensor 1,2 and CF main PWB (YC20) 4. Replace the CF adjustment sensor1,2.
    CF main PWB: Replace the CF main PWB.
  • Code: 8330
  • Description: CF blade motor error
    (4000-sheet finisher) When initial operation, CF blade sensor does not turn on within 1500 ms.
  • Remedy: CF blade motor: 1. Execute U240 Booklet — Blade to check the finisher operation . 2. Manipulate the fold blade up and down to check it is smoothly operable. 3. Check that the drive from the motor reaches the fold blade. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF blade motor and CF main PWB (YC15) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the CF blade motor.
    CF blade sensor: 1. Execute U241 Booklet — Blade HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF blade sensor and CF main PWB (YC20) 4. Replace the CF blade sensor.
    CF main PWB: Replace the CF main PWB.
  • Code: 8340
  • Description: CF staple motor error 1
    (4000-sheet finisher) Staple JAM (center-folding unit) has been detected twice in a row. (The second JAM detection condition fullfilled with the home position did not detected in 600 ms after the motor was driven.)
  • Remedy: CF staple motor: 1. Execute U240 Booklet — Staple to check the finisher operation. 2. Manipulate the staple up and down check it is smoothly operable. 3. Check that the drive from the motor reaches the staple unit. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF staple unit and CF main PWB (YC13) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the CF staple motor.
    CF staple sensor: Replace the CF staple unit.
    CF main PWB: Replace the CF main PWB.
  • Code: 8350
  • Description: CF side registration motor 1 error
    (4000-sheet finisher) When initial operation, CF side registration sensor 1 does not turn on within 1 s.
  • Remedy: CF side registration motor 1: 1. Execute U240 Booklet — Width Test to check the finisher operation. 2. Manipulate the side registration lower guide back and forth to check it can smoothly operable. 3. Check that the drive from the motor reaches the side registration lower guide. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF side registration motor 1 and CF main PWB (YC10) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the CF side registration motor 1.
    CF side registration sensor 1: 1. Execute U241 Booklet — Width Down HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF side registration sensor 1 and CF main PWB (YC20) 4. Replace the CF side registration sensor 1.
    CF main PWB Replace the CF main PWB.
  • Code: 8360
  • Description: CF main motor error
    (4000-sheet finisher) During driving the motor, the lock signal is detected for 1 s continuously.
  • Remedy: CF main motor: 1. Execute U240 Booklet — Folding to check the finisher operation. 2. Manipulate the conveying roller to check it can smoothly rotate. 3. Check that the drive from the motor reaches the conveying roller. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF main motor and CF main PWB (YC16) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the CF main motor.
    CF main PWB: Replace the CF main PWB.
  • Code: 8410
  • Description: Punch slide motor error 1
    The punch slide sensor won’t turn On when home position has been moved by 30 mm.
  • Remedy: Punch slide motor: 1. Execute U240 Booklet — Punch Move to check the finisher operation. 2. Manipulate the punch slide part of the punch unit back and forth to check it can smoothly move. 3. Check that the drive from the motor reaches punch area. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch slide motor and Punch PWB (YC3) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the punch slide motor.
    Punch slide sensor: 1. Execute U241 Punch — Punch HP to check the finisher switch. 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch slide sensor and Punch PWB (YC6) 4. Replace the punch slide sensor.
    Punch PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch PWB (YC1) and DF main PWB (YC7) (4000-sheet finisher) Punch PWB (YC1) and DF main PWB (YC8) (1000-sheet finisher) 2. Replace the punch PWB.
    DF main PWB: Replace the DF main PWB
  • Code: 8420
  • Description: Punch slide motor error 2
    In detection of paper edges, the paper edge cannot be detected in 30 mm move
  • Remedy: Punch slide motor: 1. Execute U240 Booklet — Punch Move to check the finisher operation. 2. Manipulate the punch slide part of the punch unit back and forth to check it can smoothly move. 3. Check that the drive from the motor reaches punch part. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch slide motor and Punch PWB (YC3) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the punch slide motor.
    Punch paper edge sensor 1,2: 1. Execute U241 Punch — Edge Face 1,2,3,4 to check the finisher switch . 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch paper edge sensor 1,2 and Punch PWB (YC5,YC7) 4. Replace the punch paper edge sensor 1,2.
    Punch PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch PWB (YC1) and DF main PWB (YC7) (4000-sheet finisher) Punch PWB (YC1) and DF main PWB (YC8) (1000-sheet finisher) 2. Replace the Punch PWB.
    DF main PWB: Replace the DF main PWB
  • Code: 8430
  • Description: Punch unit communication error
    Communication with the punch unit is not possible.
  • Remedy: Punch PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Punch PWB (YC1) and DF main PWB (YC7) (4000-sheet finisher) Punch PWB (YC1) and DF main PWB (YC8) (1000-sheet finisher) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Punch PWB.
    DF main PWB: Replace the DF main PWB.
  • Code: 8500
  • Description: Mailbox communication error
    (4000-sheet finisher) Communication failed to be established after the mailbox was hooked up.
  • Remedy: MB main PWB: 1. Turn the main power switch off and after 5 seconds, turn it on. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MB main PWB (YC3) and DF main PWB (YC6) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the MB main PWB.
    DF main PWB: Replace the DF main PWB.
  • Code: 8510
  • Description: MB conveying motor error 1
    (4000-sheet finisher) When initial operation, MB home position sensor does not turn on within 5 s.
  • Remedy: MB conveying motor: 1. If the transfer roller won’t rotate smoothly, repair its mechanism. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MB conveying motor and MB main PWB (YC5) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the MB conveying motor.
    MB home position sensor: 1. Execute U241 Mail Box — Motor HP to check the finisher switch . 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MB home position sensor and MB main PWB (YC2) 4. Replace the MB home position sensor.
    MB main PWB: Replace the MB main PWB
  • Code: 8520
  • Description: MB conveying motor error 2
    (4000-sheet finisher) When standby operation, MB home position sensor does not turn off within 1 s.
  • Remedy: MB conveying motor: 1. Execute Mail Box — Conv of U240 finisher operation check . 2. Manipulate the conveying roller of the mailbox to check it can smoothly rotate. 3. Check that the drive from the motor reaches the conveying roller. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MB conveying motor and MB main PWB (YC5) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the MB conveying motor.
    MB home position sensor: 1. Execute U241 Mail Box — Motor HP to check the finisher switch . 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. MB home position sensor and MB main PWB (YC2) 4. Replace the MB home position sensor.
    MB main PWB: Replace the MB main PWB.
  • Code: 8800
  • Description: Document finisher main program error
    Document finisher main program error at power up.
  • Remedy: DF main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF main PWB (YC4) and Engine PWB (YC18) (4000-sheet finisher) DF main PWB (YC7) and Engine PWB (YC18) (1000-sheet finisher) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the DF main PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB
  • Code: 8900
  • Description: Document finisher backup error
    Read and write data does not match 3 times in succession.
  • Remedy: DF main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DF main PWB (YC4) and Engine PWB (YC18) (4000-sheet finisher) DF main PWB (YC7) and Engine PWB (YC18) (1000-sheet finisher) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the DF main PWB.
  • Code: 8930
  • Description: Center-folding unit backup error
    (4000-sheet finisher) Read and write data does not match 3 times in succession.
  • Remedy: CF main PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CF main PWB (YC7) and DF main PWB (YC9) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Install the EEPROM properly. 4. Replace the CF main PWB.
  • Code: 9000
  • Description: Document processor communication error
    Communication with the document processor is not possible.
  • Remedy: DP main PWB: 1. Check that the versions of the main unit firmware and the DP firmware are identical. 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP main PWB(YC1) and ISC PWB(YC12) ISC PWB (YC3) and Main PWB (YC11) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the DP main PWB.
    ISC PWB: Replace the ISC PWB.
  • Code: 9010
  • Description: Coin vender communication error
    A communication error from coin vender is detected 10 times in succession.
  • Remedy: U206 setting: Set maintenance mode U206 to off when a coin vender is not installed .
    Coin vender control PWB: 1. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. Coin vender control PWB and Engine PWB (YC23) 2. If the wiring is disconnected, shorted or grounded, replace the wiring. 3. Replace the Coin vender control PWB.
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB .
  • Code: 9040
  • Description: DP lift motor going up error
    When the DP lift motor is driven, DP lift sensor 1 does not turn on within 1500 pulse. (Three recovery times.) The above has been detected 5 times. * : The number of detection should be weighted with one for the rise at job start and two for the irregular rise during transpoting. The accumulated number must be cleared at completion of a normal rise. The default threshold is 5.
  • Remedy: DP lift motor: 1. Execute U906 Separating Operation Release . 2. Execute U243 Lift Motor to check the DP motor operation . 3. Check that the original document lift guide can move upwards. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP lift motor and DP MAIN PWB (YC5) 5. If the wiring is disconnected, shorted or grounded, replace the wiring. 6. Replace the DP lift motor.
    DP lift sensor 1: 1. Execute U244 LIFT L-Limit to check DP switch . 2. Check that the sensor and its mounting bracket are correctly positioned. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP lift sensor 1 and DP Main PWB (YC4) 4. Replace the DP lift sensor 1.
    DP Main PWB: Replace the DP main PWB.
  • Code: 9050
  • Description: DP lift motor going down error
    When the DP lift motor is driven, DP lift sensor 2 does not turn on within 1500 pulse. (Three recovery times.) The above has been detected 5 times.
  • Remedy: DP lift motor: 1. Execute U906 Separating Operation Release . 2. Execute U243 Lift Motor to check the DP motor operation . 3. Check that the original document lift guide can move downwards. 4. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP lift motor and DP main PWB (YC5) If the wiring is disconnected, shorted or grounded, replace the wiring. 5. Replace the DP lift motor.
    DP lift sensor 2: 1. Execute U244 LIFT L-Limit to check DP switch . 2. Confirm that the DP lift sensor 2 has been firmly fitted. 3. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP lift sensor 2 and DP main PWB (YC2) 4. Replace the DP lift sensor2.
    DP main PWB: Replace the DP main PWB.
  • Code: 9060
  • Description: DP EEPROM error
    Mismatch of reading data from two locations occurs 3 times successively. Mismatch between writing data and reading data occurs 3 times successively.
  • Remedy: DP main PWB: 1. Execute U906 Separating Operation Release . 2. Confirm that the EEPROM has been properly installed. 3. Replace the DP main PWB.
    Device damage of EEPROM: Contact the Service Support.
  • Code: 9070
  • Description: Communication error between DP and SHD
    A communication error is detected.
  • Remedy: DP SHD PWB: 1. Execute U906 Separating Operation Release . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. DP SHD PWB (YC1) and DP main PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the DP SHD PWB.
  • Code: 9080
  • Description: LED fault detection
    A block is existent below a peak which was obtained by activating the LEDs in the four CIS blocks at power on, which is less than 80hex.
  • Remedy: DP CIS: 1. Execute CIS automatic original document alignment by U411 . 2. Confirm that the wiring connector is firmly connected and, if necessary, connect the connector all the way in. CIS and DP SHD PWB (YC2) DP SHD PWB (YC1) and DP main PWB (YC10) 3. If the wiring is disconnected, shorted or grounded, replace the wiring. 4. Replace the CIS and execute U411.
    DP SHD PWB: Replace the DP SHD PWB.
  • Code: 9100
  • Description: Coin vender control PWB error
    Communication error has been detected at the coin mec of the coin vender control PWB.
  • Remedy: Coin vender control PWB: Replace the coin mec.
  • Code: 9110
  • Description: Coin vender rejector error
    Communication error has been detected in connection with the coin mec and the rejector.
  • Remedy: Rejector: 1. Check that the rejector is firmly installed and, if not, install firmly. 2. Replace the rejector.
  • Code: 9120
  • Description: Sensor error in coin vender change (Yen 10)
    Change is empty despite change is enough.
  • Remedy: Coin jam in the change tube: Check visually and remedy.
    Contact in the connector: Check the connection of the empty change sensor.
    Change empty sensor: Replace the coin mec.
    Coin vender control PWB: Replace the coin mec.
  • Code: 9130
  • Description: Sensor error in coin vender change (Yen 50)
    Change is empty despite change is enough.
  • Remedy: Coin jam in the change tube: Check visually and remedy.
    Contact in the connector: Check the connection of the empty change sensor.
    Change empty sensor Replace the coin mec.
    Coin vender control PWB: Replace the coin mec.
  • Code: 9140
  • Description: Sensor error in coin vender change (Yen 100)
    Change is empty despite change is enough.
  • Remedy: Coin jam in the change tube: Check visually and remedy.
    Contact in the connector: Check the connection of the empty change sensor.
    Change empty sensor: Replace the coin mec.
    Coin vender control PWB: Replace the coin mec.
  • Code: 9150
  • Description: Sensor error in coin vender change (Yen 500)
    Change is empty despite change is enough
  • Remedy: Change tube: Check no exchange jam is observed at the outlet and, if necessary, repair it.
    Contact in the connector: Check the connection of the empty change sensor.
    Change empty sensor: Replace the coin mec.
    Coin vender control PWB: Replace the coin mec.
  • Code: 9160
  • Description: Coin vender pay-out error
    Coin is paid out despite the pay-out motor is determined not active.
  • Remedy: Pay-out motor: Replace the coin mec.
  • Code: 9170
  • Description: Coin vender pay-out sensor error
    Coin is paid out despite the pay-out motor is determined not active.
  • Remedy: Pay-out area: Check no exchange jam is observed at the outlet and, if necessary, repair it.
    Pay-out motor Replace the coin mec.
    Pay-out sensor: Replace the coin mec.
  • Code: 9500
  • Description: ISC PWB error A
  • Remedy: Main PWB, ISC PWB: 1. Reinsert the connector if its connection is loose. Main PWB (YC25) and ISC PWB (YC4) 2. Replace the main PWB . 3. Replace the ISC PWB 4. Contact the Service Support.
  • Code: 9510
  • Description: ISC PWB error B
  • Remedy: Main PWB, DP SHD PWB: 1. Reinsert the connector if its connection is loose. DP relay PWB (YC2) and DP SHD PWB (YC3) 2. Replace the main PWB . 3. Replace the DP SHD PWB. 4. Contact the Service Support.
  • Code: 9520
  • Description: ISC PWB error C
  • Remedy: Main PWB, ISC PWB: 1. Reinsert the connector if it its connection is loose. Main PWB (YC25) and ISC PWB (YC4) 2. Replace the main PWB . 3. Replace the ISC main PWB 4. Contact the Service Support.
  • Code: 9940
  • Description: Confidential document guard uninstalled error
    The confidential document guard PWB is removed while the confidential document guard PWB is valid.
  • Remedy: Confidential document guard PWB: 1. Check that the confidential document guard PWB is firmly installed and, if not, install firmly. 2. Replace the confidential document guard PW.
  • Code: 9950
  • Description: Confidential document guard PWB error
    FPGA configuration error CPU version information error This is caused when the PWB of a double-side scanning DP is connected, the confidential guard PWB is inserted, and the harness is not correctly connected.
  • Remedy: Confidential document guard PWB: 1. Replace the confidential document guard PW. 2. Replace the main PWB .
  • Code: F000
  • Description: Communication error between main PWB and operation PWB
  • Remedy: Main PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Check that the wirings and connetors between the main circuit PWB and the operation circuit PWB and between the main circuit PWB and the HDD are normal. Main PWB (YC12,YC17,YC30) and Operation PWB (YC1,YC2,YC3) 3. Check that the DDR memories in the main circuit PWB are well conducted and, if not, replace. 4. Execute U024 to initialize (FULL) the HDD . 5. Execute U021 to initialize memory. 6. Replace the Main PWB. 7. Copy the log File saved in the HDD by U964 in USB memory and contact the service support .
    Operation PWB: Replace the operation PWB .
  • Code: F010
  • Description: Main PWB checksum error
  • Remedy: Main PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. If not corrected, replace the main PWB .
  • Code: F040
  • Description: Communication error between Main PWB and Print engine
  • Remedy: Main PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Repair or replace the wire from the engine PWB, that may be grounded. (Check short-circuit between 5V and 3.3V.) 3. Check that the FCC wire connecting between the main PWB (YC3) and the engine PWB (YC46) is normal and, if necessary, re-insert.Or, replace the FCC wire. 4. If not corrected, replace the main PWB .
    Engine PWB: 1. Check the engine software and upgrade to the latest, if necessary. 2. Replace the engine PWB .
    HDD: Replace the HDD .
  • Code: F041
  • Description: Communication error between Main PWB and Scanner engine
  • Remedy: Main PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Check that the wires between the main PWB and the ISC PWB are normal. 3. If not corrected, replace the main PWB .I
    SC PWB: Replace the ISC PWB.
  • Code: F050
  • Description: Print engine ROM checksum error
  • Remedy: Engine software: Install the latest engine software.
    Engine PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Confirm that the EEPROM has been properly installed. 3. If not corrected, Replace the engine PWB .
  • Code: F051
  • Description: Scanner engine ROM checksum error
  • Remedy: Scanner software: Install the latest scanner software.
    ISC PWB: 1. Turn the main power swtch off and after 5 seconds, then turn power on. 2. Confirm that the EEPROM has been properly installed. 3. If not corrected, Replace the ISC PWB.
  • Code: F278
  • Description: Power supply in drive system error
  • Remedy: The main power switch was turned off before the power switch is pressed. Shutdown due to a power failure: Turn the main power swtch off and after 5 seconds, then turn power on. (Before turning power off, verify that the power key has been pressed and the power indicator has gone off, then switch the main power switch.)

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